摘要
通过对3根预制高强混凝土混合配筋管柱试件在不同轴压比下的拟静力试验,研究了轴压比对其抗震性能的影响.其中管柱试件中预应力钢棒和HRB400级钢筋各配置6根,两者间隔布置.详细记录试件的破坏过程,得到试件的滞回曲线、骨架曲线、承载力、变形能力、承载力退化曲线和耗能能力等.试验结果表明:各试件均为受弯破坏,延性系数为2.50~2.93,极限位移角为1/33~1/27;配置预应力筋的混合配筋管柱试件残余位移较小,自复位能力较强;轴压比是影响试件延性和耗能能力的重要因素,随着轴压比增大,试件延性降低,耗能能力减弱.
Quasi-static tests were conducted on three specimens to study the influence of axial-compression ratio on the seismic behavior of prefabricated pipe columns with high-strength concrete,which were reinforced with six prestressed steel bars and six 400,MPa grade steel bars.The failure process of specimens was recorded in detail,and several indexes such as the hysteretic curve,skeleton curve,bearing capacity,deformation capacity,stiffness degradation and energy dissipation capacity of specimens were obtained.The test results indicated that all the specimens fail in flexural mode.The ductility coefficient of the specimens is 2.50-2.93,and the ultimate drift ratio is 1/33-1/27.Pipe columns with mixed reinforcement have smaller residual displacement and better performance of automatic resilience.Axial-compression ratio is an important factor affecting the ductility and energy dissipation capacity of pipe columns.The ductility is reduced and the energy dissipation capacity is decreased with the increase of axialcompression ratio.
作者
张锡治
蔡魏巍
张潮
马健
Zhang Xizhi;Cai Weiwei;Zhang Chao;Ma Jian(Architectural Design and Research Institute of Tianjin University,Tianjin 300072,China;Civil Engineering Structure and New Materials Laboratory of Tianjin City,Tianjin University,Tianjin 300072,China;School of Civil Engineering,Tianjin University,Tianjin 300072,China)
出处
《天津大学学报(自然科学与工程技术版)》
EI
CSCD
北大核心
2017年第2期167-173,共7页
Journal of Tianjin University:Science and Technology
基金
科技部中欧合作项目(2014DFE70210)
天津市应用基础与前沿技术研究计划重点资助项目(2014JCZDJC30000)
天津市建设系统科学技术发展计划资助项目(2013-11)~~
关键词
高强混凝土管柱
混合配筋
抗震性能
延性
轴压比
pipe column with high strength concrete
mixed reinforcement
seismic behavior
ductility
axialcompression ratio