摘要
抚顺石化热电厂为自备燃煤电厂,新厂区3台锅炉均为高温高压煤粉炉。目前SO_2、NO_X烟尘的排放都无法满足《煤电节能减排升级与改造行动计划(2014—2020年)》的要求,通过对热电厂新厂区3台460t/h燃煤锅烟气进行超低排放改造,每年NO_X排放量可削减1 372t,SO_2的排放量削减594.6t,烟尘的排放量削减228t。排放烟气中NO_X<50mg/Nm^3,SO2<35mg/Nm^3,烟尘<10mg/Nm^3,达到上述国家要求。
The flue gas from the three high temperature,high pressure pulverized coal fired boilers in the self-contained coal-power plant in Petrochina Fushun petrochemical company could not meet the requirements of " Action Plan for the Low-emission and Energy Conservation Upgrade for Coal Power Plants (2014-2020)".In this study,the practice of the ultra-low emission transformation on the three 640 t/h boilers were introduced.After the transformation,the annual NOx emissions could be reduced by 1 372 t,SO 2 emissions by 594.6 t,and smoke emissions by 228 t.The concentration of NOx was less than 50 mg/Nm^3,the concentration of SO 2 was less than 35 mg/Nm^3,and the concentration of smoke was less than 10 mg/Nm 3.The upgrade of the boilers could ensure that the flue gas meet the emission standards.
作者
刘娇
Liu Jiao(Department of Quality,Safety and Environmental Protection,PetroChina Fushun Petrochemical Company)
出处
《油气田环境保护》
CAS
2019年第2期42-45,62,共5页
Environmental Protection of Oil & Gas Fields