摘要
对HT2井套管分级箍脱扣事故进行了深入调查研究,依据落鱼状况设计了引锥,采取对扣插入的方式及时处理了分级箍脱扣事故。依据套管柱插入配合接头后的连接强度和密封性能及对落鱼管柱变形损坏状态分析结果,给出了后续钻水泥塞和钻井过程应采取的措施,防止套管磨损,并对原套管设计扣型提出了改进建议。
This paper gives an investigation on tripping accident of casing stage collar in well HT2.The guide cone was designed according to fished casing joint,and the tripping accident of grading hoop was dealt with in time by inserting the buckle.Based on analysis on joint strength and sealing performance of insert connection,and on deformation and damage of fished casing string,it was suggested that prevention measure from casing wear should be taken,and that the original casing connection design should be improved.
作者
滕学清
杨向同
朱金智
吕拴录
杨成新
TENG Xueqing;YANG Xiangtong;ZHU Jinzhi;LYU Shuanlu;YANG Chengxin(PetroChina Tarim OilField Company,Korla,Xinjiang 841000,China;Material Science and Engineering Department of China University of Petroleum,Beijing 102249,China)
出处
《石油管材与仪器》
2019年第3期45-48,共4页
Petroleum Tubular Goods & Instruments
关键词
固井
脱扣
落鱼
对扣
引锥
well cementation
trip
fish
stab
guide cone