摘要
催化裂化油浆中固体催化剂粉末的脱除是当前油浆深加工过程中普遍面临的一个技术难题。为了实现油浆的深度净化,提高油浆的综合利用价值,某公司2.30Mt/a催化裂化装置首次工业应用JR-SA06高效油浆脱灰剂。应用结果表明:在脱灰剂相对外甩油浆添加量(w)为500μg/g、沉降温度为90~95℃的试验条件下,经过72h沉降后,油浆灰分由0.28%降至0.019%,平均脱灰率达到了93.16%,优于一般脱灰剂,为油浆的后续加工利用创造了良好的条件。
The removal of solid catalyst powder from FCC slurry is a common technical challenge in the deep processing of FCC slurry.To realize deep purification for slurry and to improve the comprehensive utilization value of the slurry, the JR-SA06 efficient slurry deash agent was first applied in 2.3 Mt/a FCC unit of a company.The application results demonstrated that adding 500μg/g deash agent based on the FCC slurry and settling at 90-95 ℃ for 72 hours,the ash content in the slurry decreased from 0.28% to 0.019%,removal rate of ash reached 93.16%,which is superior to the common deash agents and creates good conditions for the subsequent processing and utilization of slurry.
作者
黄辉明
杨成武
马庆功
李辉
Huang Huiming;Yang Chengwu;Ma Qinggong;Li Hui(Fujian Refining & Petrochemical Co.Ltd.,Quanzhou , Fujian 326800;Jilin Jurun Environmental Protection Technology Co.Ltd.)
出处
《石油炼制与化工》
CAS
CSCD
北大核心
2019年第11期21-25,共5页
Petroleum Processing and Petrochemicals