摘要
S12梅龙高速公路K24+615深度3号桥2014年通车运营后,在车辆动荷载及梁体本身纵向下滑力的作用下,第一联(0#~5#墩)左幅梁体向梅州方向纵向位移5~7cm,右幅梁体向梅州方向纵向位移3~5cm,影响行车安全。通过对第一联偏移梁体整体顶升和对支座进行改造后,同步顶推纠偏使梁体恢复到原设计位置。
After Shendu No.3 Bridge at K24+615 of S12 Meilong Expressway was opened to traffic in 2014,under the action of the vehicle dynamic load and the longitudinal sliding force of the beam itself,5~7cm longitudinal displacement of the direction to Meizhou appeared at the first joint(0#~5#pier)left beam,and the longitudinal displacement of the right beam body to Meizhou is 3~5cm,which have affected the safety of traffic.After reconstruction of bearing with whole lifting of the first joint beam,the synchronous thrust correction has restored the beam to the original design position.
作者
王博
WANG Bo(Guangdong Changda Road Maintenance Co.,Ltd.,Guangzhou 510620)
出处
《广东公路交通》
2019年第5期111-115,共5页
Guangdong Highway Communications
关键词
纵向偏移
整体顶升
支座改造
梁体纠偏
longitudinal slip
integral jacking up
bearing transformation
beam rectification