摘要
研究区主要管辖的XJ长7、LX长4+5等致密、超低渗透油藏开发矛盾突出,注水不见效,地层能量逐年下降,低产低效油井占比大。本文通过对2018年在该区摸索试验油井挤活性水112井次进行综合效果评价,对该技术在不同油藏的适应性进行总结,为下步低产低效井治理,油藏提单产、降递减,老油田稳产提供思路。
The main of the study area is XJ Chang 7,LX Chang 4+5 and other dense or ultra-low permeability reservoirs,and the contradiction is prominent.The water injection is not effective,the formation energy is decreasing year by year,and the low-production and low-efficiency oil wells account for a large proportion.The paper evaluates the comprehensive effect of the injecting activated water technology in different oil reservoirs in 2018,summarizes the adaptability of the technology in different reservoirs,and provides ideas for the management low-production and low-efficiency wells,the reduced of reservoirs declining,and the stable production of old oilfields.
作者
刘喆
张翠萍
李龙龙
胡文超
杨兴海
王鹏
腊丹萍
薛璇
范敬敬
LIU Zhe;ZHANG Cuiping;LI Longlong;HU Wenchao;YANG Xinghai;WANG Peng;LA Danping;XUE Xuan;FAN Jingjing(Oil Production Plant 6 of PetroChina Changqing Oilfield Company,Dingbian Shaanxi 718606,China)
出处
《石油化工应用》
CAS
2019年第11期64-69,74,共7页
Petrochemical Industry Application
关键词
挤活性水
增油
致密油
解堵
稳产
injecting activated water
enhanced production
the tight oil
plugging removal
stable productions