摘要
TUD-DNS3脱硝助剂在中韩(武汉)石油化工有限公司1号催化裂化装置上进行了工业应用。结果表明:针对两段再生工艺,当系统中助剂占总催化剂藏量的质量分数为2.6%时,烟气脱硫装置外排污水中的氨氮质量浓度由加剂前的100 mg/L下降至40 mg/L以内;助剂的加入降低了CO焚烧炉的炉膛温度,有利于烟气的合格排放,并对装置操作、产品分布及汽油、柴油产品质量无不良影响。
The commercial application of denitration additive TUD-DNS3 in FCC unit of SINOPEC-SK(Wuhan)Petrochemical Co.Ltd.was introduced.The results demonstrated that when the mass fraction of this additive accounted for 2.6%of total catalyst inventory,the ammonia nitrogen content in the effluent water of flue gas desulfurization unit reduced from 100 mg/L to less than 40 mg/L;the addition of additive lowered the furnace temperature of CO incinerator,and the emission of flue gas was qualified.No adverse effect on the operation of the plant,the product distribution and the qualities of gasoline and diesel products were found.
作者
蔡筱青
涂安斌
Cai Xiaoqing;Tu Anbin(SINOPEC-SK(Wuhan)Petrochemical Co.Ltd.,Wuhan 430081)
出处
《石油炼制与化工》
CAS
CSCD
北大核心
2020年第2期20-24,共5页
Petroleum Processing and Petrochemicals
关键词
脱硝助剂
催化裂化
氨氮
denitration additive
fluid catalytc cracking
ammonia nitrogen