摘要
元坝天然气净化厂采用UDS-Ⅱ复合溶剂脱除天然气中的H 2S、CO 2及有机硫等杂质,产品天然气达到国家标准GB 17820—2012《天然气》一类气指标。随着国家环保要求日益提高,2018年国家颁发新版GB 17820—2018《天然气》标准,元坝天然气净化厂现有工艺无法满足新标准要求。为此,根据元坝净化厂天然气脱硫工艺及产品气的特点,增设COS水解或分子筛精脱硫设施的方案均能有效提升产品质量,满足了新国标的要求。若进一步降低产品气总硫含量,还需加大对天然气净化工艺的开发力度才能实现。
UDS-II complex solvent is used by Yuanba Natural Gas Treating Plant to remove impurities such as H 2S,CO 2 and organic sulfur in the raw natural gas.The treated gas can meet the first class specification of Natural Gas(GB 17820—2012).With the more and more stringent environmental protection requirements in China,a new edition of Natural Gas(GB 17820—2018)was issued in 2018 and the natural gas product of Yuanba Natural Gas Treating Plant couldn’t meet the requirements of the new standard.Combined with the characteristics of the natural gas desulfurization process and the natural gas product of the plant,the impact of the new standard on the plant was analyzed.Additional COS hydrolysis or molecular sieve desulfurization facilities can effectively improve the product quality and meet the requirements of the new standard.To further reduce the total sulfur content of natural gas product,the development of natural gas treating technology shall be strengthened continuously.
作者
李健
邱云霞
李林龄
Li Jian;Qiu Yunxia;Li Linling(SINOPEC Engineering Incorporation,Beijing,100101;SINOPEC Guangyuan Natural Gas Treating Plant,Sichuan,Guangyuan,628400)
出处
《石油化工设计》
CAS
2020年第1期40-43,I0004,共5页
Petrochemical Design
关键词
天然气脱硫
分子筛
COS水解
复合溶剂
natural gas desulfurization
molecular sieve
COS hydrolysis
complex solvent