摘要
中国石化达州天然气净化有限公司天然气净化厂二联合第二系列(122系列)20 kt/a硫磺回收单元自2018年4月起开始使用国产TiO2基克劳斯催化剂LS-981G进行工业试验。装置运行一年的实践结果表明:国产TiO2基克劳斯催化剂LS-981G具有良好性能,羰基硫总水解率在98%以上,CS2总水解率为100%,总硫回收率在99.96%以上,烟气中SO2排放质量浓度低于400 mg/m^3,远低于GB 16297—1996《大气污染物综合排放标准》中SO2质量浓度不大于960 mg/m^3的指标。
The second unit with a capacity of 20 kt/a(122 series)for sulfur recovery in the No.2 complex unit of Natural Gas Purification Plant of SINOPEC Dazhou Natural Gas Purification Co.Ltd.has started industrial trials using domestic TiO2-based Claus catalyst LS-981G since April 2018.The practical results of the device running for one year showed that the catalyst LS-981G had a good performance,the total hydrolysis rate of carbonyl sulfur was above 98%,the total hydrolysis rate of carbon disulfide was 100%,and the total sulfur recovery rate was above 99.96%.The mass concentration of SO2 in the flue gas emission was less than 400 mg/m3,which is far lower than the reqirement(not exceeding 960 mg/m3)of the GB 16297—1996“Comprehensive Air Pollutant Emission Standard”.
作者
胡良培
张文斌
杜莉
魏荆辉
黄坤
Hu Liangpei;Zhang Wenbin;Du Li;Wei Jinghui;Huang Kun(Natural Gas Purification Plant,SINOPEC Dazhou Natural Gas Purification Co. Ltd.,Dazhou,Sichuan 635000)
出处
《石油炼制与化工》
CAS
CSCD
北大核心
2020年第3期38-42,共5页
Petroleum Processing and Petrochemicals