摘要
介绍了改良天然气吹硫工艺原理及其在硫磺回收装置上的应用情况。该工艺从以下两个方面进行改良:①使用天然气和氮气的混合气体进行停工,通过制硫炉掺入氮气增加停工期间载硫、载热气量,缩短停工时间;②通过计算确定停工过程配风量,避免设备、催化剂局部超温,应用改良天然气吹硫停工工艺,中国石化北京燕山分公司60 kt/a硫磺回收装置在未设置烟气后碱洗塔的情况下,成功地将停工吹硫、钝化期间尾气焚烧炉排放的烟气中SO 2质量浓度控制在100 mg/m^3以内,实现了达标排放。该改良工艺具有显著的社会效益,可以进一步推广应用。
This paper introduces the principle of improved shutdown process by using natural gas and its application on sulfur recovery unit.The process was improved from following aspects:(1)A mixture of natural gas and nitrogen for shutdown was used.The addition of nitrogen into the Claus furnace increased the amount of sulfur and heat-carrying gas during the shutdown period and shortened the downtime.(2)The air distribution during the shutdown process was determined through calculation to avoid over-temperature of the equipment and catalysts.The industrial application of Sinopec Beijing Yanshan Branch 60 kt/a sulfur recovery unit showed that the flue gas SO 2 mass concentration emitted from the tail gas furnace during shutdown and blowing could be controlled within 100 mg/m^3 without setting caustic wash tower,which reached the discharge standard.The improved process has significant social benefits which can be further promoted and applied.
作者
郑晓薇
魏在兴
Zheng Xiaowei;Wei Zaixing(SINOPEC Beijing Yanshan Branch,Beijing,China)
出处
《石油与天然气化工》
CAS
CSCD
北大核心
2020年第2期8-13,共6页
Chemical engineering of oil & gas
关键词
硫磺回收
达标排放
天然气
吹硫
停工
sulfur recovery
discharge to reach standard
natural gas
blow off residual sulfur
shutdown