摘要
为了解决煤层气多分支水平井分支井眼因重入困难、不能下入筛管、无法实现筛管完井的问题,研制了空心结构的筛管完井重入引导工具,优选了煤层气多分支水平井完井方式,给出了分支井眼重入筛管完井施工步骤,形成了煤层气多分支水平井分支井眼重入筛管完井技术。该技术在沁试12平1井的现场试验结果表明,对比重入引导工具与钻进时MWD测得的井眼轨迹数据可判断是否重入成功,筛管能顺利通过筛管完井重入引导工具下至分支井眼,实现分支井眼筛管完井。研究结果表明,煤层气多分支水平井分支井眼重入筛管完井技术,解决了煤层气水平井分支井眼无法重入、不能实现筛管完井的问题。
In order to solve problems caused by difficult re-entry of branched boreholes in CBM multi-lateral horizontal wells,such as the inability to RIH screen and the impossibility to realize the screen completion,a re-entry guide tool for screen completion with hollow structure was developed,the completion technology for multi-lateral borehole in CBM multi-lateral horizontal wells was optimized,and the steps of re-entry screen completion for multilateral borehole were proposed,thereby forming the re-entry screen completion technology for multi-lateral CBM horizontal wells.The technology was tested in Well Qinshi 12-1;and the test results showed that by comparing the re-entry guide tool with the borehole trajectory data measured by MWD,and it could be judged whether the re-entry was successful,and the screen could be RIH to the branched wellbore to achieve the screen completion.The results also showed that the re-entry screen completion technology for multi-lateral CBM horizontal wells solved the problems of difficult re-entry and the screen completion.
作者
谭天宇
李浩
李宗源
蒋海涛
何景朝
TAN Tianyu;LI Hao;LI Zongyuan;JIANG Haitao;HE Jingchao(Engineering Technology Research Institute,BHDC,CNPC,Renqiu,Hebei,062550,China;Coalbed Methane Division,Huabei Oilfield Company,Renqiu,Hebei,062550,China)
出处
《石油钻探技术》
CAS
CSCD
北大核心
2020年第4期78-82,共5页
Petroleum Drilling Techniques
基金
国家科技重大专项“煤层气新型水平井钻完井关键技术与工具研究”(编号:2016ZX05022-004)
“沁水盆地高煤阶煤层气高效开发示范工程”(编号:2017ZX05064)联合资助。
关键词
煤层气
水平井
多分支井
筛管完井
沁试12平1井
coalbed methane
horizontal well
multi-lateral well
screen completion
Well Qinshi 12-1