摘要
京隆发电公司2×600 MW机组为满足灵活调峰的要求,采用省煤器热水再循环技术路线对1号机组进行宽负荷脱硝改造。通过改造,达到了机组30%BMCR及以上负荷工况下脱硝系统连续投运的目的,可为同类型机组深度调峰宽负荷脱硝改造提供参考。
In order to meet the requirements of flexible peak regulation,2×600 MW units of Jinglong power generation company are denitrified with wide load.Through the reformation of economizer hot water recirculation,the denitrification system is continuously put into operation under the load condition of 30%BMCR and above,providing certain reference for denitrification reformation of units of the same type with deep and wide load.
作者
王荣
王晓风
王耀
WANG Rong;WANG Xiaofeng;WANG Yao(Inner Mongolia Jinglong Power Generation Co.,Ltd.,Ulanqab,Inner Mongolia 012100,China;Xinjiang Oilfield Company Emergency Rescue Center,Karamay,Xinjiang 834000,China)
出处
《东北电力技术》
2020年第9期19-21,共3页
Northeast Electric Power Technology
关键词
锅炉
宽负荷脱硝
入口烟温
改造
经济效益
boiler
wide-load denitration
inlet smoke temperature
modification
economic benefit