摘要
在脱磷理论分析基础上,采用低枪位冶炼和低终点氧出钢,增大出钢口直径和降低终点温度,并优化底吹工艺降低碳氧积,取得了较好的脱磷效果。生产应用结果表明:采用增大出钢口和优化底吹工艺后,300 t转炉出钢时间缩短至5.1 min,缩短了1.9 min;IF钢终点温度降低至1 670.6℃,降低了17.4℃;碳氧积降低至13.3,降低了8.9;终点氧降低至422.5×10^(-6)。在铁水磷升高0.010%,枪位降低30 cm,终点氧降低153.3×10^(-6)的条件下,工艺优化后的平均终点磷含量为0.012 4%,能够满足转炉冶炼IF钢对脱磷效果的要求。
On the basis of theoretical analysis of dephosphorization,by using low lance position smelting and low endpoint oxygen tapping,increasing diameter of tapping hole and reducing the end-point temperature,and optimizing bottom blowing process to reduce the carbon-oxygen equilibrium,a better dephosphorization effect is achieved.The results of production and application show that after adopting large tapping hole and optimizing bottom blowing process,the tapping time of 300 t converter is shortened to 5.1 min,shortened by 1.9 min;the end-point temperature of IF steel is reduced to1670.6℃,reduced by 17.4℃;the carbon-oxygen product is reduced to 13.3,reduced by 8.9;the end-point oxygen is reduced to 422.5×10-6.Under the condition of increase of hot metal phosphorus by 0.010%,decrease of lance position by 30 cm and decrease of end-point oxygen by 153.3×10-6,the average end-point phosphorus content after process optimization is reduced to 0.0124%,which can meet the requirements of dephosphorization effect of IF steel smelting in converter.
作者
邱在军
Qiu Zaijun(NO.4 Steelmaking and Rolling General Plant of Masteel Co Ltd,Ma'anshan 243000)
出处
《特殊钢》
北大核心
2020年第6期51-54,共4页
Special Steel
关键词
300T转炉
脱磷
出钢时间
终点温度
碳氧积
终点氧
300t BOF
Dephosphorization
Tapping Time
End-Point Temperature
Carbon-Oxygen Equilibrium
End-Point Oxygen