摘要
针对西昌钢钒半钢冶炼钢水及炉渣氧化性高带来的透气砖侵蚀快、底吹效果不佳的问题,通过对底吹供气元件优选、优化透气砖布置方案以及热更换方案,提高了全炉役底吹搅拌效果。工业应用表明,底吹工艺参数优化后,透气砖热更换时间平均缩短95 min,炼钢转炉全炉役钢-渣间LP由78.0提高到92.5,终渣TFe质量分数由19.7%降低到18.6%,终点钢水碳氧积由0.0028降低到0.0023,在提高转炉生产效率的同时,降低了冶炼成本。
To solve the problem of low bottom blowing effect and fast erosion of bottom tuyeres caused by high oxidability of slag during semi-steel steelmaking in Pangang Group Xichang Vanadium&Steel Co.,Ltd.,measures such as application of new bottom blowing tuyeres,optimization of bottom tuyeres arrangement and optimization of thermal-replacement scheme were adopted.Bottom blowing effect during the converter campaign was improved.Industrial application indicated that after the optimization of bottom blowing process,mean thermal-replacement time was shorten by 95 min,average phosphor distribution ratio(LP)between steel-slag during the whole converter campaign was improved from 78.0 to 92.5,mean TFe mass fraction in end-point slag was reduced form 19.7%to 18.6%,and average carbon-oxygen concentration product at end-point was reduced from 0.0028 to 0.0023.Production efficiency of converter steelmaking was improved and cost of BOF blowing was reduced as well.
作者
陈均
CHEN Jun(State Key Laboratory of Vanadium and Titanium Resources Comprehensive Utilization,Pangang Group Research Institute Co.,Ltd.,Panzhihua 617000,China)
出处
《炼钢》
CAS
北大核心
2020年第5期21-26,36,共7页
Steelmaking
关键词
半钢冶炼
数值模拟
底吹
碳氧积
semi-steel steelmaking
numerical simulation
bottom blowing
carbon-oxygen equilibrium