摘要
针对M区块部分气井增压效果变差的问题,开展泡沫排水采气工艺辅助增压开采试验研究。通过改进泡排流程及起泡剂用量优化调整,经现场应用,试验气井稳产、增产、助排效果显著,优化后的单井雾化消泡流程现场效果较好。试验表明,起泡剂加注量应实行一井一制,根据实际情况不断调整优化。
Aiming at the problem of poor pressurization effect of some gas wells in M Block,the foam drainage gas recovery process was used to assist pressurized mining.By improving the foaming drainage process and optimizing the amount of foaming agent,the test gas wells had a significant effect on stable production,increasing production,and drainage assistance.The optimized single well atomization defoaming process had a good field effect.Test results have shown that the amount of foaming agent should be one well for one strategy,and continuously adjusted and optimized according to actual conditions.
作者
陈晓宇
姜宇玲
李牧
李凌君
杜家澄
CHEN Xiaoyu;JIANG Yuling;LI Mu;LI Lingjun;DU Jiacheng(Sinopec Chongqing Fuling Shale Gas Exploration and Development Co.,Ltd.,Chongqing 408014,China;Exploration and Development Research Institute,Sinopec Jianghan Oilfield Company,Wuhan 430223,China)
出处
《复杂油气藏》
2020年第3期77-80,共4页
Complex Hydrocarbon Reservoirs
基金
国家科技重大专项“涪陵页岩气开发示范工程”(2016ZX05060)。
关键词
天然气开发
泡沫排水采气
增压开采
natural gas development
foam drainage gas recovery
pressurized mining