期刊文献+

超长冲程抽油机在低渗透油田的应用评价

Evaluation of the applicability of ultra-long stroke pumping unit in low permeability oilfields
下载PDF
导出
摘要 长庆低渗透油田具有产液量低、井斜大、井深的特点,主要采用的游梁式抽油机举升工艺具有耗电高、系统效率低、泵效低,井筒偏磨严重的问题。为解决油田提质增效的瓶颈性问题,通过调研论证,开展了超长冲程采油技术高效举升试验,试验结果表明:超长冲程抽油机较常规技术在泵效、系统效率方面具有较明显的优势,技术经济性和节能降耗效益较好,可扩大试验规模。 Changqing low permeability oilfield has the characteristics of low fluid production,large well slope and deep well.The main beam pumping unit lifting process has the problems of high power consumption,low system efficiency,low pump efficiency and serious shaft eccentric wear.In order to solve the bottleneck problem of improving quality and the efficiency,conducted a super long stroke recovery technique efficient lifting test through the research.The test results show that the super long stroke pumping unit a conventional technology in the pump efficiency and system efficiency has the obvious advantage,technology economy and better energy saving benefit,can expand the scale of the test.
作者 赵春 姚洋 杜向前 赵勇 梁毅 辛宏 雷雨 张磊 魏韦 罗聪英 张岩 呼苏娟 ZHAO Chun;YAO Yang;DU Xiangqian;ZHAO Yong;LIANG Yi;XIN Hong;LEI Yu;ZHANG Lei;WEI Wei;LUO Congying;ZHANG Yan;HU Sujuan(Oil and Gas Technology Research Institute of PetroChina Changqing Oilfield Company,Xi'an Shaanxi 710018,China;National Engineering Laboratory for Exploration and Development of Low Permeability Oil and Gas Fields,Xi'an Shaanxi 710018,China;Oil Production Plant 3 of PetroChina Changqing Oilfield Company,Yinchuan Ningxia 750006,China;Longdong Headquarters of PetroChina Changqing Oilfield Company,Xifeng Gansu 745000,China)
出处 《石油化工应用》 CAS 2021年第4期36-39,共4页 Petrochemical Industry Application
基金 中国石油集团公司长庆油田科技项目“超长冲程抽油机适应性及生产配套技术研究”,项目编号:2020DD010。
关键词 长冲程 人工举升 评价 long stroke artificial lift evaluation
  • 相关文献

参考文献6

二级参考文献24

共引文献12

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部