摘要
消力池内常因消能不足而引起水流流态紊乱、临底流速大、出池后有二次水跃等问题。结合某待建水利工程,开展了带尾墩的新型综合消力池水流特征试验研究。通过对比原方案与9个优化方案,得到以下结论:在消力池尾坎上设置差动式尾墩后,下泄水流分多股支流进行纵向和横向扩散消能,水流流态稳定,消能率增大。消力池加深1 m、加宽4 m且增加差动式尾墩的消能方案消能效果明显,池内形成稳定淹没水跃,出池后二次水跃现象明显消除。
The conventional stilling pool often causes flow instabilities in the pool,secondary water jumps after exiting the pool and high velocity near the bottom due to insufficient energy dissipation within the pool.The water flow characteristics of a new type of integrated stilling pool with tail piers are studied for a certain practical project.The original design scheme is compared with nine optimized schemes,and the results show that,when the differential tail pier is installed on the tail sill of the stilling pool,the discharge water is diffused longitudinally and laterally into multiple tributary streams,and there is no large fluctuation for the water surface,the flow pattern is stable and the energy dissipation rate is evidently increased.The scheme which will deepen the pool by 1 m,widen the pool by 4 m and set differential tail pier has best energy dissipation effect,and can form a stable submerged hydraulic jump within the pool and eliminate the secondary hydraulic jump at the downstream of the pool.
作者
杨姣
刘亚坤
张帝
段双帅
岑嘉豪
刘春明
YANG Jiao;LIU Yakun;ZHANG Di;DUAN Shuangshuai;CEN Jiahao;LIU Chunming(School of Hydraulic Engineering,Faculty of Infrastructure Engineering,Dalian University of Technology,Dalian 116024,Liaoning,China)
出处
《水力发电》
CAS
2021年第9期132-137,共6页
Water Power
基金
国家自然科学基金资助项目(51909024)
辽宁省自然科学基金(ZX20190526、20180540132)
辽宁省重点实验室科研专题基金(DUT19LAB35)。
关键词
水流流态
临底流速
差动式尾墩
二次水跃
综合消力池
消能率
flow pattern
underflow speed
differential tail pier
second hydraulic jump
integrated stilling pool
energy dissipation