期刊文献+

某发动机张紧器故障原因分析及前端轮系优化

Analysis of Tensioner’s Malfunction and Optimization on Engine Front End Accessory Drive System
下载PDF
导出
摘要 针对某发动机空调-发电机层自动张紧器故障率高问题,将其与风扇-水泵层轮系进行对比分析,张紧器故障率高是由张紧臂摆角过大导致的。通过优化,将空调-发电机层轮系由曲轴驱动改为风扇托架驱动,通过计算优化后空调-电机层轮系的张紧臂摆角降低到0.5°以下,并通过市场验证,证实了方案的有效性。 Aiming at the high failure rate of the automatic tensioner in the air-conditioner-generator gear train of an engine,it is found that the high failure rate of the tensioner is caused by the excessive swing angle of the tensioner arm by comparing it with the fan-pump gear train.Through optimization,the air-conditioner and generator gear train was changed from crankshaft drive to fan carrier drive.After calculation,the swing angle of the tensioning arm of the air-conditioner and generator gear train was reduced to less than 0.5°,and the validity of the scheme was verified by market verification.
作者 曾超 王俊然 刘伦伦 王景新 尚嘉丽 ZENG Chao;WANG Junran;LIU Lunlun;WANG Jingxin;SHANG Jiali(State Key Laboratory of Engine Reliability,Shandong Weifang 261061;Weichai Power Co.,Ltd.,Shandong Weifang 261061)
出处 《汽车实用技术》 2021年第17期80-83,87,共5页 Automobile Applied Technology
关键词 FEAD系统 自动张紧器 张紧臂 激励源 阻尼比 Front end accessory drive system Automatic tensioner The tension arm Excitation source Damping ratio
  • 相关文献

参考文献4

二级参考文献14

  • 1刘际仁,葛红.多楔带自动张紧器简介[J].内燃机,2005,21(2):46-49. 被引量:14
  • 2吴昕.多楔带轮系的布置、计算和寿命分析[J].汽车技术,1997(2):5-11. 被引量:21
  • 3Shangguan WB, Zeng XK. Experimental and calculation analysis of rotational vibration responses for an engine front end accessory drive system: Part I. Experiments and mea- surement results. ASME Journal of Vibration and Acous- tics, 2013, 135(3): 031002/1-14.
  • 4Hwang S J, Perkins NC, Ulsoy AG, et al. Rotational re- sponse and slip prediction of serpentine belt drives systems. Journal of Vib,ation and Acoustics, 1994, 6(1): 71-78.
  • 5Zhao JX, Barker C. Experimental testing and modeling of automotive automatic belt tensioners. SAE paper, 980839.
  • 6Cheng G, Zu WJ. Nonstick and stick-slip motion of a coulomb-damped belt drive system subjected to multifre- quency excitations. ASME Journal of Applied Mechanics, 2003, 70(6): 871-884.
  • 7Bastien, J, Michon, G, Manin, L. et al. An analysis of the modified Dahl and Masing models: application to b belttensioner. Journal of Sound and Vibration, 2007, 302(6): 841-864.
  • 8Michon G: Manin L: Dufour R. Hysteretic behavior of a belt tensioner: modeling and experimental investigation. Journal of Vibration and Control, 2005, 11(9): 1147-1158.
  • 9李承谦.柴油机前端附件驱动系统的设计[J].柴油机设计与制造,2008,15(1):14-15. 被引量:5
  • 10赵晓芬,周盛,郑志镇.UG二次开发在皮带轮设计中的应用[J].煤矿机械,2008,29(12):194-196. 被引量:4

共引文献21

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部