摘要
为提高煤矿顺层钻孔瓦斯抽采效果,通过对水力压裂机理及影响因素分析,在该矿进行定向水力压裂实验,布置4个压裂钻孔,2个导向钻孔,脉动频率20 Hz。实验结束后,对瓦斯抽采浓度及流量进行观测,与普通顺层钻孔相比,导向钻孔、压裂钻孔的瓦斯抽采浓度和流量均有明显提高,说明水力压裂可以促使煤层渗透率增加、透气性增强,有助于瓦斯预抽。
In order to improve the gas drainage effect of coal mine drilling along the bed,through the analysis of hydraulic fracturing mechanism and influencing factors,a directional hydraulic fracturing experiment was carried out in this mine,and 4 fracturing holes and 2 pilot holes were arranged,and the pulsation frequency was 20 Hz.After the experiment,the gas drainage concentration and flow rate were observed.Compared with the ordinary bedding drilling,the gas drainage concentration and flow rate of the pilot hole and the fracturing hole were significantly improved,indicating that hydraulic fracturing could promote the coal seam.Increased permeability and enhanced air permeability helped gas pre-pumping.
作者
郭陇飞
GUO Long-fei(Zuoquanfu Raw Coal Industry Co.,Ltd.,Shanxi Lu′an Group,Jinzhong 032600,China)
出处
《煤炭科技》
2022年第2期120-122,127,共4页
Coal Science & Technology Magazine
关键词
瓦斯抽采
水力压裂
瓦斯浓度
瓦斯流量
gas extraction
hydraulic fracturing
gas concentration
gas flow