摘要
针对涪陵页岩气储层钻塞效率低、事故风险高等问题,通过室内实验、理论研究以及现场数据分析,开展了连续油管泡沫钻塞技术研究。通过优选起泡剂与稳泡剂,最终确定泡沫钻塞液的配方为1.2%起泡剂JY+0.15%稳泡剂HPAM,并对钻塞工艺的磨鞋与螺杆马达等关键工具以及排量、钻压、上提速度等关键参数进行了优化。该技术在8口井进行了现场应用,与传统方法相比,钻塞时效提高79.8%,事故率降低51.5%。该技术可有效提高页岩气钻进效率,降低事故率,具有推广应用价值。
Aiming at the problems of low drilling efficiency and high accident risk in Fuling shale gas reservoir,the foam drilling technology of coiled tubing was studied through laboratory experiment,theoretical research and field data analysis. By optimizing foaming agent and stabilizing agent,the formulation of foam drilling fluid was finally determined as 1.2 % foaming agent JY+0.15 %stabilizing agent HPAM. Key tools,such as shoe grinding and screw motor,as well as key parameters,such as displacement,bit pressure and lifting speed,were optimized for the corresponding foam drilling plug process. The technology was used in eight wells and resulted in a 79.8% increase in plug timings and a 51.5% reduction in accident rates compared to conventional methods. The application results show that this technology can effectively improve the work efficiency of shale gas drilling,reduce the accident rate,and has application and promotion value.
作者
于洋
YU Yang(Downhole Special Service Company of Zhongyuan Petroleum Engineering Co.,Ltd.,SINOPEC,Puyang 457164,China)
出处
《复杂油气藏》
2022年第2期90-96,共7页
Complex Hydrocarbon Reservoirs
基金
山东省优秀青年基金(ZR2020YQ36)资助。
关键词
连续油管
钻塞
泡沫钻塞液
钻磨工艺
coiled tubing
drilling plug
foam drill plug fluid
drilling and milling-grinding technology