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基于振动抑制的发动机进气畸变耙研制

Development of intake distortion rake based on vibration suppression
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摘要 针对航空发动机进气流场压力畸变测试需求,基于耙臂的振动抑制,首次采用浮动内环连接结构,研制了一种发动机进气畸变测试耙。强度计算结果表明,所设计的进气畸变测试耙的动、静强度均有足够的储备裕度。测频试验和动应力测试试验结果表明,内环与耙臂连接结构对进气畸变测试耙整体振动抑制效果明显。进气畸变测试耙工程应用效果良好,可满足发动机进发匹配以及进气逼喘试验的需求。 Based on the pressure distortion measurement of aero-engine inlet,a float connection structure was designed and the pressure distortion rake of aero-engine was investigated based on the vibration sup⁃pression.The results of structural strength calculation show that the rake meet the measurement require⁃ments.The results of frequency measurement and dynamic stress measurement show that the float connec⁃tion structure is conducive to the vibration suppression of distortion rake.The engineering application effect of rake was ideal,which can satisfy the requirements of engine/inlet matching and surge test.
作者 张校东 万媛媛 薛秀生 王晓良 刘忠奎 ZHANG Xiao-dong;WAN Yuan-yuan;XU Xiu-sheng;WANG Xiao-liang;LIU Zhong-kui(AECC Shenyang Engine Research Institute,Shenyang 110015,China;Chongqing Institute of Aerospace Propulsion Technology,Chongqing 401120,China)
出处 《燃气涡轮试验与研究》 2022年第1期58-62,共5页 Gas Turbine Experiment and Research
关键词 航空发动机 进气畸变耙 振动抑制 浮动连接 强度计算 测频试验 动应力测试 aero-engine intake distortion rake vibration suppression float connection strength calculation frequency measurement dynamic stress measurement
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  • 1孟庆迪,罗贵火,王少华.某型飞机进气道测压总耙振动模态分析[J].振动工程学报,2004,17(z2):892-894. 被引量:2
  • 2[2]龚曙光.ANSYS基础应用及范例分析.北京:机械工业出版社,2002
  • 3《航空发动机设计手册》总编委会.进排气装置[M].北京:航空工业出版社,2000:222-225.
  • 4Yuhas A J,Ray R J,Burley R R,et al. Design and Development of an F/A-18 Inlet Distortion Rake: A Cost and Time Saving Solution[R]. NASA TM-4722, 1995.
  • 5Amin N F,Hollweger D J. F/A-18A Inlet/Engine Compatibility Flight Test Results [R]. AIAA 81-1393, 1981.
  • 6吴国钏,等.附面层理论[M].北京:航空工业出版社,1989.
  • 7Trong T Bui, David L Oates. Design and evaluation of a new boundary layer rake for flight testing[ J]. NASA TM - 2000 - 209014,2000.
  • 8Richwine David M. F - 15B/Flight test fixture: a test bed for flight research[ J]. NASA TM -4782,1996.
  • 9Laurie A Marshall. Boundary layer transition results from the F - 16XL - 2 supersonic laminar flow control experiment [ J]. NASA TM - 1999 - 209013,1999.
  • 10Yuhas A J, Ray R J, Burley R R, et al. Design and Development of an F/A-18 Inlet Distortion Rake:A Cost and Time Saving Solution [R]. NASA TM- 4722, 1995.

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