摘要
针对20CrMnTi钢入轧钢加热炉出现自然断裂的问题,对铸坯的横向断口进行分析,结果表明主要原因是铸坯的凹陷和浇铸时二冷区域回温。通过调整保护渣的理化指标及优化结晶器水量,减少二冷回温等改进措施,改善了铸坯的凹陷,连续20个浇次5.46万t铸坯在入轧钢加热炉过程未出现自然断裂。
Aiming at the problem of natural fracture of 20CrMnTi steel entering the rolling reheating furnace, the transverse fracture of slab was analyzed.The results show that the main reasons are the depression of the billet and the temperature return in the secondary cooling area during casting.By adjusting the physical and chemical indexes of protective slag and optimizing the water volume of crystallizer, improvement measures such as reducing secondary cooling return temperature, the depression of billet was improved, and 54 600 tons of billet was poured for 20 consecutive times without natural fracture in the process of entering the rolling reheating furnace.
作者
胡贺亚
王吾磊
黄雁
杨仁强
李海
邓齐根
HU He-ya;WANG Wu-lei;HUANG Yan;YANG Ren-qiang;LI Hai;DENG Qi-gen(Wuhu Xinxing Ductile Iron Pipe Co.Ltd.Steelmaking Department,Wuhu 241070,China)
出处
《甘肃冶金》
2023年第1期23-26,共4页
Gansu Metallurgy