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一种快速接钻杆方法在大功率电液钻机的应用

Application of a quick drill pipe connection method in high-power electro-hydraulic drilling rigs
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摘要 针对大功率电液钻机钻杆取放和钻杆拧卸(统称接钻杆)耗时长、效率低的问题,提出了一种快速接钻杆方法。为了实现快速下钻接钻杆,采用一种机械臂闭环联动和动力头同步上扣方法:接收到下钻接钻杆指令后,机械大臂、机械横梁和动力头同时动作,当钻杆在移动过程中与动力头和主夹持器干涉(碰撞),机械横梁停止动作,动力头继续后退,远离主夹持器,当干涉解除,机械横梁继续移动直至到位后,机械大臂和机械小臂联动,将钻杆自上而下快速放入中部上卸区域,当正转压力达到预设值10 MPa,钻杆丝扣啮合结束。考虑提钻接钻杆为连续循环动作,采用差值位移同步法:通过计算机械抓手径向缩回和机械横梁轴向位移差值,有效解决动力头与钻杆丝扣松开过程中,机械臂抓放钻杆时间过长、干涉等问题。当机械抓手径向升高300 mm时,与机械横梁轴向位移差值越大越安全,在动力头松开前扣完成后,机械臂复位,控制结束。工业性试验结果表明,该快速接钻杆方法的下钻接钻杆、提钻接钻杆用时分别较常规方法节省179,41 s,整体下钻接钻杆、提钻接钻杆成功率分别较常规方法提高22.3%,19.1%。 In order to solve the problem of long time consumption and low efficiency in the pickup and placement and unscrewing of the drill pipe screw(drill pipe connection)on high-power electro-hydraulic drilling rigs,a quick drill pipe connection method is proposed.To achieve quick drilling and drill pipe connection,a method of closed loop linkage of the manipulator and power head synchronization on the buckle is adopted.After receiving the command for drilling and drill pipe connection,the mechanical arm,mechanical beam,and power head act simultaneously.When the drill pipe interferes(collides)with the power head and main holder during the curve trajectory movement,the mechanical beam stops acting.And the power head continues to retreat away from the main holder.When the interference is removed,after the mechanical beam continues to move until it is in place,the manipulator large arm and small arm are linked to quickly place the drill pipe into the middle loading and unloading area from top to bottom.When the forward rotation pressure reaches the preset value of 10 MPa,the screw engagement of the drill pipe ends.Aiming at the continuous cyclic action of lifting and connecting the drill pipe,the differential displacement synchronization method is adopted.By calculating the difference between the radial retraction of the mechanical grip and the axial displacement of the beam,the problems such as excessive time and interference of the manipulator in grasping and releasing the drill pipe during the loosening process of the power head and drill pipe threads are effectively solved. When the mechanical grip radially rises by 300 mm, the greater the difference in axial displacement from the mechanical beam, the safer it will be. After the power head releases the front buckle, the manipulator resets and control ends. The results of industrial tests show that compared with conventional methods, the average time saved by this quick drill pipe connection method for drilling down and drill pipe connection and lifting and drill pipe connection is 179 s and 41 s respectively, and the success rates of overall drilling down and drill pipe connection and lifting and drill pipe connection have increased by 22.3% and 19.1% respectively.
作者 邢望 李芬 王宁芳 李冬生 李旺年 XING Wang;LI Fen;WANG Ningfang;LI Dongsheng;LI Wangnian(CCTEG Xi'an Research Institute(Group)Co.,Ltd.,Xi'an 710077,China;Xi'an Gloden Mountain Ceramic Composites,Xi'an 710072,China;National Key Laboratory of Thermostructure Composite Materials,School of Materials Science and Engineering,Northwestern Polytechnical University,Xi'an 710072,China)
出处 《工矿自动化》 CSCD 北大核心 2023年第4期128-133,共6页 Journal Of Mine Automation
基金 陕西省重点研发计划资助项目(2023-YBGY-340)。
关键词 大功率电液钻机 下钻接钻杆 提钻接钻杆 钻杆取放 钻杆拧卸 闭环控制 high-power electrohydraulic drilling rig drilling down and drill pipe connection lifting and drill pipe connection drill pipe pickup and placement drill pipe unscrewing closed-loop control
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