摘要
为了响应国家节能减排政策,降低企业经营成本,某电厂在准确测量风量的基础上,对其300 MW等级循环流化床锅炉机组进行了优化运行调整。结果表明,优化后飞灰含碳量平均降低了1.44%,底渣含碳量平均降低了0.36%,尿素日均耗量平均降低了1.54 t,月均厂用电率降低了0.16%,预计全年可以实现经济效益近750万元。
In order to respond to the national energy conservation and emission reduction policy and reduce the operating cost of enterprises,a power plant has optimized the operation of its 300 MW circulating fluidized bed boiler unit on the basis of accurate measurement of air volume.The results showed that the carbon content of fly ash decreased by 1.44%and bottom slag decreased by 0.36%respectively after optimization.The average daily urea consumption decreased by 1.54 t.The average monthly auxiliary power consumption rate decreased by 0.16%.It is estimated that the annual economic benefits can reach nearly 7.5 million yuan.
作者
赵阳
李健奇
李含琼
王美旭
董浩宇
ZHAO Yang;LI Jianqi;LI Hanqiong;WANG Meixu;DONG Haoyu(Liaoning Dongke Electric Power Co.,Ltd.,Shenyang,Liaoning 110179,China;Beijing Runke Tongyong Technology Co.,Ltd.,Beijing 100080,China;Beijing Zhongdian Changfeng Energy Saving Technology Co.,Ltd.,Beijing 100020,China;Shenyang Jinshan Energy Co.,Ltd.,Shenyang,Liaoning 110101,China)
出处
《东北电力技术》
2023年第5期59-62,共4页
Northeast Electric Power Technology
关键词
风量测量
循环流化床锅炉
优化运行
飞灰含碳量
air volume measurement
circulating fluidized bed boiler
optimized operation
carbon content of fly ash