摘要
YC1井生产套管破损,需进行取换套管作业。针对深部取换套管的特点,借鉴封隔器式套管对接方法的优点,设计了Ø178 mm套管外插筒工具,制定相应的施工工艺,通过提断、回接、切割、取出旧套管,经过修磨鱼顶、新旧套管对接及注水泥固井、钻水泥塞、试压等工序,成功取换Ø139.7 mm生产套管2 499.85 m,刷新中石化取换套管最长纪录,为深井取换套管提供了成功经验。
The production casing of well YC1 was damaged and the casing removal and replacement operation was required.According to the characteristics of deep casing removal and replacement,combined with the advantages of packer type casing docking method,aØ178 mm casing outer casing tool is designed and developed,and corresponding construction technological measures are put into practice.Through lifting off,tie-back,cutting,taking out the old casing,after repairing and grinding the“fish top”,butting the old and new casing,cementing,drilling cement plugs,and pressure test,etc.,2499.85 m ofØ139.7 mm production casing was successfully removed and replaced,which set a new record for the longest casing removal in Sinopec Group,and provided a successful experience for deep well casing removal and replacement.
作者
黄志安
吴波
王委
陈金国
HUANG Zhi’an;WU Bo;WANG Wei;CHEN Jinguo(Jiangsu Drilling Company of Huadong Petroleum Engineering Co.Ltd.,SINOPEC,Yangzhou 225000,China;Huadong Petroleum Engineering Co.Ltd.,SINOPEC,Nanjing 210019,China)
出处
《复杂油气藏》
2023年第2期230-233,共4页
Complex Hydrocarbon Reservoirs
基金
中石化工程公司重大科技项目“东部老油田勘探开发配套工程关键技术”子课题“大斜度井和小尺寸套管开窗侧钻提速技术的研究与应用”(编号:SG1706-05K)资助。
关键词
套管破损
套管切割
回接
外插筒
YC1井
casing damage
casing cutting
casing tie-back
external cartridge
well YC1