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某砌体结构房屋桩基托换顶升纠倾工程实例

JACKING AND TILTING PROJECT OF A MASONRY STRUCTURE THROUGH PILE FOUNDATION REPLACEMENT
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摘要 以某多层砌体结构住宅楼顶升纠倾工程为研究对象,该楼整体倾斜率达13.4‰,已远超出规范允许值。通过新增人工挖孔桩对原结构基础进行托换加固,采取后注浆技术解决桩端持力层渗水问题,然后以人工挖孔桩作为顶升反力平台,运用PLC液压同步顶升控制系统对建筑物进行整体纠倾,纠倾后使结构整体倾斜率降至1‰,施工效果良好,对今后类似工程项目具有借鉴意义。 Taking a multi–storey masonry residential building jacking and tilting project as the research object,the overall tilt rate of the building is 13.4‰,which has far exceeded the standard allowable value.In this paper,the original structure foundation was replaced by adding new artificially bored piles,and the problem of water seepage in the bearing layer at the pile end was solved by post–grouting technology,and then the building was tilted by using PLC hydraulic synchronous jacking control system with artificially bored piles as the jacking reaction platform.After the tilt correction,the overall tilt rate of the structure was reduced to 1‰,and the construction effect was good,which is of reference for similar projects in the future.
作者 周健男 夏巍 李业龙 吴东光 赵晓玉 ZHOU Jian-nan;XIA Wei;LI Ye-long;WU Dong-guang;ZHAO Xiao-yu(Hebei Building Research Engineering Co.,Ltd.,050200,Shijiazhuang,China)
出处 《建筑技术》 2023年第24期3006-3008,共3页 Architecture Technology
基金 2022年河北省建设科技研究项目(2022–2070)。
关键词 顶升 纠倾 桩基托换 后注浆技术 jacking up jacking and tilting pile foundation replacement post grouting technology
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