摘要
采用初始铸造工艺试制的ZM6镁合金“Z”字型复杂薄壁筒形壳体铸件出现夹渣、疏松缺陷。对缺陷产生的原因进行分析后,通过对铸件浇注系统和激冷系统的优化设计,确定了合理的工艺方案。采用优化后的铸件成型工艺方案,最终解决了铸件的夹渣、疏松缺陷问题,且铸件内部、外观品质均符合技术要求,取得了良好的技术经济效果。
The initial casting process design scheme for the Z-shaped complex thin-walled cylindrical shell casting of ZM6 magnesium alloy showed defects such as slag inclusion and porosity in the trial production results.After analyzing the causes of defects,by optimizing the design of the casting pouring system and chilling system,a reasonable process plan has been determined.By adopting the optimized casting forming process plan,the problems of slag inclusion and porosity defects in the castings were ultimately solved,and the internal and external quality of the castings met the technical requirements,achieving good technical and economic results.
作者
汪华兵
WANG Huabing(Guizhou Anji Aviation Investment Casting Co.,Ltd.,Anshun 561000,Guizhou China)
出处
《铸造工程》
2024年第S01期12-15,共4页
Foundry Engineering
关键词
ZM6
镁合金
铸造工艺
浇注系统
激冷系统
缺陷
ZM6
magnesium alloy
casting process
pouring system
chilling systems
defects