摘要
在中海石油宁波大榭石化有限公司22万t/a催化裂解(DCC)装置上进行了重整碳五油回炼的工业试验。结果表明:回炼过程中装置运行稳定,在提升管出口温度为620℃的条件下,重整碳五油转化率为42.90%,其中纯碳五转化率为25.65%;回炼重整碳五油后,DCC装置干气中的乙烯体积分数增加了0.55个百分点,丙烯收率增加了0.12个百分点。
The industrial test of refining reformed C_(5) oil recycle was carried out in a 220 kt/a deep catalytic cracking(DCC)unit of Ningbo Daxie Petrochemical Co Ltd,CNOOC.The results showed that the unit ran stably during the refining process,under the condition of the outlet temperature of the riser at 620℃,the conversion rate of reformed C_(5) oil was 42.90%,of which the conversion rate of pure C_(5) oil was 25.65%.After refining reformed C_(5) oil,the ethylene volume fraction in dry gas of DCC unit increased by 0.55 percentage point,and the propylene yield increased by 0.12 percentage point.
作者
张诚
ZHANG Cheng(Production Technology Department of Ningbo Daxie Petrochemical Co Ltd,CNOOC,Ningbo 315812,China)
出处
《石化技术与应用》
CAS
2024年第4期287-288,297,共3页
Petrochemical Technology & Application
关键词
催化裂解
重整碳五油
回炼
乙烯
丙烯
deep catalytic cracking
reformed C_(5) oil
refining
ethylene
propylene