摘要
大港油田赵东CP3-D18-XX井为一口水平生产井,其中完钻井深3064 m,水平位移2288 m,ϕ244.5 mm套管下入至2998.69 m。该井311.1 mm井眼裸眼段长,井眼轨迹复杂且清洁困难,导致套管下入摩阻大,套管下入悬重不足,采用常规下套管方式无法下入到位。结合漂浮下套管与顶驱下套管工艺的特点,采用漂浮+顶驱下套管工艺技术,完成ϕ244.5 mm套管下入工作。通过现场应用及评价,在常规下套管方法不满足施工要求时,推荐在水平井中采用漂浮+顶驱下套管工艺,不仅可以克服套管下入摩阻大、大勾载荷不足等问题,在遇阻时还可快速旋转活动套管,极大降低了下套管黏卡风险,保障了现场作业安全。
CP3-D18-XX,a horizontal production well in Dagang Zhaodong Oilfield,has a total depth of 3064 m and a horizontal displacement of 2288 m,with the setting depth ofϕ244.5 mm casing reaching 2998.69 m.Due to the long open hole with a diameter of 311.1 mm,complex borehole trajectory,and the difficulty in hole cleaning,the casing running process encountered high friction resistance and insufficient suspended load,failing to succeed using the conventional method.The technologies of floating and top drive casing running were combined forϕ244.5 mm casing running.The on-site application and evaluation show that this comprehensive technology is recommended when conventional casing running methods cannot meet the operation requirements.It can not only overcome problems such as high resistance and insufficient hook load of casing running but also quickly rotate retrievable casings to reduce the risk of casing sticking,ensuring the safety of on-site operation.
作者
张浩
沈吉阳
李洪奎
ZHANG Hao;SHEN Jiyang;LI Hongkui(Drilling Branch of CNPC Offshore Engineering Company Limited,Tianjin 065000,China)
出处
《石油工程建设》
2024年第S01期1-7,共7页
Petroleum Engineering Construction
关键词
水平井
漂浮下套管
顶驱下套管
horizontal well
floating casing running
top drive casing running