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1000MW火力发电机组容量电价测试下氧量偏低的原因分析及控制措施

Analysis and Control Measures for Low Oxygen Content in Capacity Electricity Pricing Test of 1000MW Thermal Power Generation Unit
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摘要 为适应新能源的发展,促使煤电向基础保障性和调节性电源并重转型,保障电力系统安全稳定。2024年1月1日江苏省正式执行容量电价补偿机制,为保障最高出力达标调用,各机组均需具备带满出力能力。但因长周期运行,2号机组在夏季时,存在氧量低的问题,对机组安全造成一定影响。通过本文,结合实际情况,提出解决控制措施,为机组满出力达标调用提供了借鉴作用。 In order to adapt to the development of new energy and promote the transformation of coal-fired power to both basic and regulated power sources,ensuring the safety and stability of the power system.On January 1,2024,Jiangsu Province officially implemented the capacity electricity price compensation mechanism.In order to ensure that the maximum output meets the standard,each unit must have the ability to operate at full capacity.However,due to long-term operation,Unit 2 suffers from low oxygen levels during summer,which has a certain impact on the safety of the unit.Through this article,combined with the actual situation,control measures are proposed to provide reference for the full output standard call of the unit.
作者 贾兴贵 孙姣姣 JIA Xing-gui;SUN Jiao-jiao(State Power Investment Group GCL Binhai Power Generation Co.,Ltd.Yancheng 224000,China;Yancheng Thermal Power Co.,Ltd.Yancheng 224000,China)
出处 《全面腐蚀控制》 2024年第12期34-36,共3页 Total Corrosion Control
关键词 容量电价 达标调用 安全稳定 氧量 capacity electricity price standard call safe and stable oxygen content
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