摘要
中石化股份有限公司济南分公司混合床 -催化蒸馏甲基叔丁基醚装置原采用轻C4 作原料 ,1998年为了降低生产成本改用混合C4 作原料 ,由于混合C4 原料中杂质及C5含量高 ,出现催化剂失活较快及MTBE产品纯度下降等问题 ,通过分析和试验 ,采取反应器前增设净化器、调整催化蒸馏塔操作参数等措施 ,抑制了催化剂的失活和副反应的产生 ,生产出了合格的MTBE产品。
In order to decrease production cost, mixed C 4 fraction was used in the mixed phase bed-catalytic distillation MTBE unit in SINOPEC Ji nan Company as feedstock in stead of light C 4 fraction in 1998. However, the high content of impurities and C 5 fraction in mixed C 4 fraction caused problems such as quick deactivation of catalyst and decreasing of the purity of MTBE products.After taking measures such as adding a purifier in front of the reactor, adjusting operating parameters of the catalytic distillation tower, etc., the deactivation of catalyst and side reactions were controlled, and qualified product MTBE is produced.
出处
《齐鲁石油化工》
2002年第4期314-317,共4页
Qilu Petrochemical Technology