摘要
红安 1 1 0 k V站增装无功补偿间隔后 ,3 60 0 kvar并补电容器不能投运。在故障分析的基础上进行改造 ,使之恢复正常投运 。
After adding the reactive power compensation bay at Hongan 110kV substation,the 3 600kvar capacitors couldn′t be into service.On the basis of fault analyzing and reforming,it worked normally and its availability was increased.
出处
《湖北电力》
2002年第5期1-2,共2页
Hubei Electric Power