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某井油管变扣短节断裂原因分析 被引量:2

Causes Analysis on the Fracture of the Tubing Joint in an Oil Well
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摘要 某井油管变扣短节服役5个月即发生断裂失效。通过对失效油管变扣短节的宏观形貌、微观形貌、理化性能进行分析和检验,查明了其断裂原因。结果表明:该油管变扣短节断裂主要是由硫化氢应力腐蚀开裂导致的;由于该井硫化氢含量较高,因此建议该井油管柱采用抗硫材料。 The tubing joint in an oil well fractured only used for five months,and the fracture reasons were analyzed by observing its macro and micro morphology and testing its physical and chemical properties.The results show that the fracture of the tubing joint was mainly caused by sulfide stress corrosion cracking.Because the hydrogen sulfide content in the oil well was rather high,sulfur resistant material was suggested to be used.
出处 《理化检验(物理分册)》 CAS 2015年第10期730-732,共3页 Physical Testing and Chemical Analysis(Part A:Physical Testing)
关键词 油管变扣短节 断裂 硫化物应力腐蚀开裂 tubing joint fracture sulfide stress corrosion cracking
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  • 1API SPEC 5CT-2001套管和油管规范[S].
  • 2API SPEC 8C-1997钻井与采油提升设备规范[S].

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