摘要
某型涡轮螺桨发动机曾发生过多起转子偏磨故障,工厂对此作过许多分析,本文在其基础上再对该项故障的原因和机理结合实际地作了进一步的比较、分析和论证,提出了排故措施。效果显著。
In this paper the troubleshooting is performed for a certain type of turboprop engine starting under 'hot state', in which the blades in one side of the compressor rotor seriously rub the case at a speed near and lower than the idling speed. The measurements of vibration characteristics for both trouble free and trouble engines starting under both 'hot state' and 'cold state' were made. The measured vibration signals were analyzed with a frequency spectrum analyzer. Based on the comparison between the experimental results and the calculated dynamic characteristics it is believed that the rotor shaft is deformed and bent due to the uneven temperature distribution around the shaft as starting under 'hot state . and there exists a critical speed near and lower than the idling speed of the engine . The nonlinear response of the bent rotor appears due to the nonlinear stiffness of the flexible front support of the compressor rotor under the relatively high load, the amplitude rises continually after the rotor passes the conventional critical speed, and then leads to the fault described above. Some suggestions for remedying the frouble were have been given. Such failures are reduced significantly after some of the remedial measures were taken.
出处
《航空学报》
EI
CAS
CSCD
北大核心
1992年第10期B512-B516,共5页
Acta Aeronautica et Astronautica Sinica
关键词
转子
热弯曲
非线性
涡桨发动机
rotor, 'hot state', critical speed, nonlinear response