摘要
红南边底水油田在开采过程中出现了锥进问题,通过应用侧钻水平井新技术治理底水锥进获得了成功,提高了区块开发效果,获得了较好经济效益,为同类油藏的开发提供了可借鉴经验。
Sidetracking horizontal wells were used successfully to control the water coning occurred in Hongnan oil field, hence the development and the economy benefits of the block were improved. This provided reference for the development of similar reservoirs.
出处
《吐哈油气》
2003年第1期46-47,共2页
Tuha Oil & Gas
关键词
侧钻水平井
红南油田
底水
锥进
治理
sidetracking horizontal well
Hongnan oil field
bottom water
water coning
control
effectiveness