摘要
炼油厂污水经A2/O为核心的生化系统处理后,水质可达到污水综合排放标准。有效利用炼油厂低温余热,通过负压多效蒸发工艺实现净化后污水的回收再利用,是炼油厂节能减排的新举措。进水水质中硅、浊度是蒸发工艺防垢、控制水质的主要参数,以硅、浊度的同步去除为目标,研究了石灰、镁盐沉淀、铁铝盐共沉淀法对硅和浊度去除效果的影响。结果表明,当Ca(OH)2的投加量为500mg/L时,硅、浊度的同步去除率分别为79.2%和4.2%;pH值=10.0,MgCl2投加量为400mg/L时,硅、浊度的同步去除率分别为91.6%和74.4%;优选的Fe(Ⅱ/Ⅲ)Al复合混凝剂投加量为400mg/L时,硅、浊度的同步去除率分别为91.9%和90.4%。Fe(Ⅱ/Ⅲ)Al复合混凝剂作用效果满足蒸发系统对进水硅和浊度的控制要求,处理后硅含量为17.93mg/L,浊度为3NTU。
The oil refinery effluent was dealt with biochemical treatment taking A2/O as a core,and its quality could reach the comprehensive discharge standard of effluent.The effluent could be recycled by the low pressure multi-effect evaporation system using the low temperature heat of oil refinery,and it was the new measure of energy saving and emission reduction.The silicon and turbidity were the main parameters of evaporation process.The removal effect of silicon and turbidity by softening with lime,magnesium salt precipitation and precipitation by combination coagulant of molysite and aluminium salt were researched.The results indicated that:when the dosage of Ca(OH)2was 500mg/L,the removal rate of silicon and turbidity were 79.2%and4.2%,respectively,and when the dosage of MgCl2 was 400mg/L at the pH value of 10,the removal rate of silicon and turbidity were 91.6%and 74.4%,respectively.The requirement of low temperature multi-effect evaporation system could be achieved,when the dosage of Fe(Ⅱ/Ⅲ)Al combination coagulant was 400mg/L and the removal rate of silicon and turbidity were 91.9%and 90.4%,respectively.The residual silicon content and turbidity were 17.93 mg/L and 3NTU.
出处
《石油与天然气化工》
CAS
CSCD
2014年第3期326-330,共5页
Chemical engineering of oil & gas
基金
中国石油低碳重大专项"含油污泥资源化利用技术集成"(2011E-2407)
关键词
炼油废水
低温多效蒸发
混凝剂
脱硅除浊度
oil refinery effluent,low temperature multi-effect evaporation,coagulation,silicon and turbidity removal