摘要
在GDX6S设备运行过程中经常发生商标胶缸检测器不能正确测出胶缸储胶量,在胶缸胶水使用到最低水平以下时,胶缸注胶口不能及时得到指令添加胶水,导致设备出现“错误涂胶的商标纸”故障停机,为解决此问题提出一种在检测孔处加装下端开口的内衬管,并定时在内衬管中加水的方法。应用效果表明,改造后的GDX6S包装机出现“错误涂胶的商标纸”故障停机频次由改造前的15.4次/台/天下降到3.6次/台/天,改进效果显著。
In the process of operation of GDX6S equipment, the trademark glue cylinder detector cannot correctly determine the amount of glue stored in the cylinder. When the glue cylinder is used below the minimum level, the glue injection port cannot be instructed to add glue in time, resulting in the failure and shutdown of the trademark paper with wrong glue application. In order to solve this problem, a method is put forward to install the inner liner with lower opening at the detection hole, and add water to the inner liner regularly. The application effect showed that the stopping frequency of the malfunctioning of the mis-gluing trademark paper on the modified GDX6S pack-aging machine decreased from 15.4 times/day before the modification to 3.6 times/day of each machine, and the improvement effect was remarkable.
出处
《仪器与设备》
2018年第4期140-147,共8页
Instrumentation and Equipments