FCC units are playing an important role at refineries, in particular at Chinese refineries. To cope with the current demand for better economic benefits, environmental protection and product slate adjustment, a host o...FCC units are playing an important role at refineries, in particular at Chinese refineries. To cope with the current demand for better economic benefits, environmental protection and product slate adjustment, a host of FCC units need to be technically revamped. This article describes the practical processes, technologies and equipment to serve different revamp targets with analysis of two examples on revamp of commercial units.展开更多
PetroChina Karamai Petrochemical Branch Company by means of the technology licensed by UOP has revamped the cyclone system, feed nozzles, and main air distribution pipe of the 500 kt/a FCC unit, resulting in reduced c...PetroChina Karamai Petrochemical Branch Company by means of the technology licensed by UOP has revamped the cyclone system, feed nozzles, and main air distribution pipe of the 500 kt/a FCC unit, resulting in reduced coke formation and decreased dry gas yield in this unit. On the basis of the existing equipment, the throughput of this unit has been increased to 800 kt/a from 500 kt/a, with the total liquid yield reaching 88.66%. In the meantime, the revamp has reduced the pressure drop in the regenerator system with apparent energy conservation effects and significant economic benefits.展开更多
文摘FCC units are playing an important role at refineries, in particular at Chinese refineries. To cope with the current demand for better economic benefits, environmental protection and product slate adjustment, a host of FCC units need to be technically revamped. This article describes the practical processes, technologies and equipment to serve different revamp targets with analysis of two examples on revamp of commercial units.
文摘PetroChina Karamai Petrochemical Branch Company by means of the technology licensed by UOP has revamped the cyclone system, feed nozzles, and main air distribution pipe of the 500 kt/a FCC unit, resulting in reduced coke formation and decreased dry gas yield in this unit. On the basis of the existing equipment, the throughput of this unit has been increased to 800 kt/a from 500 kt/a, with the total liquid yield reaching 88.66%. In the meantime, the revamp has reduced the pressure drop in the regenerator system with apparent energy conservation effects and significant economic benefits.