Using ball milling and single direction pressing, we can produce high performance NdFeB sintered magnets. The oxygen content of sintered magnets can be controlled under 1500xl0^-6 and the magnetic performance can be i...Using ball milling and single direction pressing, we can produce high performance NdFeB sintered magnets. The oxygen content of sintered magnets can be controlled under 1500xl0^-6 and the magnetic performance can be improved by using low oxygen processing. The high preformance NdFeB sintered magnets with Br=(1.4 ± 0.2)T, iHc>796 kA/m and (BH)max=(390± 16) kJ/m^3, have been batch produced.展开更多
A full-scale test was operated by using low dissolved oxygen activated sludge process to enhance biological nitrogen and phosphorus removal. When the influent concentrations of CODCr, TN and TP varied in a range of 35...A full-scale test was operated by using low dissolved oxygen activated sludge process to enhance biological nitrogen and phosphorus removal. When the influent concentrations of CODCr, TN and TP varied in a range of 352.9 mg/L-1338.2 mg/L, 34.4 mg/L-96.3 mg/L, and 2.21 mg/L-24.0 mg/L, the average removal efficiencies were 94.9%, 86.7% and 93.0%, respectively. During the test period of two months, effluent meas of CODCr,, BOD5, NH3-N, TN and TP were below 50 mg/L, 25 mg/L, 10 mg/L and 1.0 mg/L respectively. The low dissolved oxygen activated sludge process has a simple flow sheet, fewer facilities and high N and P removal efficiency. It is very convenient to retrofit the conventional activated sludge process with the above process.展开更多
文摘Using ball milling and single direction pressing, we can produce high performance NdFeB sintered magnets. The oxygen content of sintered magnets can be controlled under 1500xl0^-6 and the magnetic performance can be improved by using low oxygen processing. The high preformance NdFeB sintered magnets with Br=(1.4 ± 0.2)T, iHc>796 kA/m and (BH)max=(390± 16) kJ/m^3, have been batch produced.
文摘A full-scale test was operated by using low dissolved oxygen activated sludge process to enhance biological nitrogen and phosphorus removal. When the influent concentrations of CODCr, TN and TP varied in a range of 352.9 mg/L-1338.2 mg/L, 34.4 mg/L-96.3 mg/L, and 2.21 mg/L-24.0 mg/L, the average removal efficiencies were 94.9%, 86.7% and 93.0%, respectively. During the test period of two months, effluent meas of CODCr,, BOD5, NH3-N, TN and TP were below 50 mg/L, 25 mg/L, 10 mg/L and 1.0 mg/L respectively. The low dissolved oxygen activated sludge process has a simple flow sheet, fewer facilities and high N and P removal efficiency. It is very convenient to retrofit the conventional activated sludge process with the above process.