Dual-fuel premixed charge compression ignition (DF-PCCI) combustion has been proven to be a viable alternative to conventional diesel combustion in heavy-duty compression ignition engines due to its low nitrogen oxide...Dual-fuel premixed charge compression ignition (DF-PCCI) combustion has been proven to be a viable alternative to conventional diesel combustion in heavy-duty compression ignition engines due to its low nitrogen oxides (NOx) and particulate matter (PM) emissions. When natural gas (NG) is applied to a DF-PCCI engine, its low reactivity reduces the maximum pressure rise rate under high loads. However, the NG–diesel DF-PCCI engine suffers from low combustion efficiency under low loads. In this study, an injection strategy of fuel supply (NG and diesel) in a DF-PCCI engine was investigated in order to reduce both the fuel consumption and hydrocarbon (HC) and carbon monoxide (CO) emissions under low load conditions. A variation in the NG substitution and diesel start of energizing (SOE) was found to effectively control the formation of the fuel–air mixture. A double injection strategy of diesel was implemented to adjust the local reactivity of the mixture. Retardation of the diesel pilot SOE and a low fraction of the diesel pilot injection quantity were favorable for reducing the combustion loss. The introduction of exhaust gas recirculation (EGR) improved the fuel economy and reduced the NOx and PM emissions below Euro VI regulations by retarding the combustion phasing. The combination of an NG substitution of 40%, the double injection strategy of diesel, and a moderate EGR rate effectively improved the combustion efficiency and indicated efficiency, and reduced the HC and CO emissions under low load conditions.展开更多
This paper examines the effect of equalizing ignition delay in a compression ignition engine.Two sets of tests were conducted,i.e.a set of constant injection timing tests with start of fuel injection at 10°crank ...This paper examines the effect of equalizing ignition delay in a compression ignition engine.Two sets of tests were conducted,i.e.a set of constant injection timing tests with start of fuel injection at 10°crank angle degree(CAD)before top dead center(BTDC)and a set of constant ignition timing tests while also keeping the 10℃AD BTDC injection and adding ignition improver(2-ethylhexylnitrate-,2-EHN)to the fuel mixtures.Soot particles were characterized using DMS-500 instrument in terms of mass,size,and number.The experimental results showed that adding 2-EHN to the model fuel blends reduced the soot surface area,soot mass concentration and soot mean size.Replacing 20 vol%of a C 7-heptane with 20 vol%methyl-decanoate(an oxygenated C 11 molecule)did not affect the ignition delay or rate of fuel air premixing,the peak in-cylinder pressure or heat release rates.Toluene addition(0−22.5 vol%)to heptane increased the mean size of the soot particles generated by only 3%while also resulted in a slight increase in the peak cylinder pressure and peak heat release rates.Blending toluene and methyl-decanoate into heptane without adding 2-EHN increased the premix phase fraction by at least 13%.However,by adding 2-EHN(4×10^(−4)−1.5×10^(−3)),the premixed phase fraction decreased by at least 11%.展开更多
基金the Global-Top Project,Development of Advanced Combustion Technology for Global Top Low Emission Vehicle(2016002070001)the Ministry of Environment(MOE)of Korea for financial support by the Center for Environmentally Friendly Vehicle(CEFV)
文摘Dual-fuel premixed charge compression ignition (DF-PCCI) combustion has been proven to be a viable alternative to conventional diesel combustion in heavy-duty compression ignition engines due to its low nitrogen oxides (NOx) and particulate matter (PM) emissions. When natural gas (NG) is applied to a DF-PCCI engine, its low reactivity reduces the maximum pressure rise rate under high loads. However, the NG–diesel DF-PCCI engine suffers from low combustion efficiency under low loads. In this study, an injection strategy of fuel supply (NG and diesel) in a DF-PCCI engine was investigated in order to reduce both the fuel consumption and hydrocarbon (HC) and carbon monoxide (CO) emissions under low load conditions. A variation in the NG substitution and diesel start of energizing (SOE) was found to effectively control the formation of the fuel–air mixture. A double injection strategy of diesel was implemented to adjust the local reactivity of the mixture. Retardation of the diesel pilot SOE and a low fraction of the diesel pilot injection quantity were favorable for reducing the combustion loss. The introduction of exhaust gas recirculation (EGR) improved the fuel economy and reduced the NOx and PM emissions below Euro VI regulations by retarding the combustion phasing. The combination of an NG substitution of 40%, the double injection strategy of diesel, and a moderate EGR rate effectively improved the combustion efficiency and indicated efficiency, and reduced the HC and CO emissions under low load conditions.
文摘This paper examines the effect of equalizing ignition delay in a compression ignition engine.Two sets of tests were conducted,i.e.a set of constant injection timing tests with start of fuel injection at 10°crank angle degree(CAD)before top dead center(BTDC)and a set of constant ignition timing tests while also keeping the 10℃AD BTDC injection and adding ignition improver(2-ethylhexylnitrate-,2-EHN)to the fuel mixtures.Soot particles were characterized using DMS-500 instrument in terms of mass,size,and number.The experimental results showed that adding 2-EHN to the model fuel blends reduced the soot surface area,soot mass concentration and soot mean size.Replacing 20 vol%of a C 7-heptane with 20 vol%methyl-decanoate(an oxygenated C 11 molecule)did not affect the ignition delay or rate of fuel air premixing,the peak in-cylinder pressure or heat release rates.Toluene addition(0−22.5 vol%)to heptane increased the mean size of the soot particles generated by only 3%while also resulted in a slight increase in the peak cylinder pressure and peak heat release rates.Blending toluene and methyl-decanoate into heptane without adding 2-EHN increased the premix phase fraction by at least 13%.However,by adding 2-EHN(4×10^(−4)−1.5×10^(−3)),the premixed phase fraction decreased by at least 11%.