A novel, highly linear sampling switch suitable for low-voltage operation is proposed. This switch not only eliminates the nonlinearity introduced by gate-source voltage variation, but also reduces the nonlinearity re...A novel, highly linear sampling switch suitable for low-voltage operation is proposed. This switch not only eliminates the nonlinearity introduced by gate-source voltage variation, but also reduces the nonlinearity resuiting from threshold voltage variation, which has not been accomplished in earlier low-voltage sampling switches. This is achieved by adopting a replica transistor with the same threshold voltage as the sampling transistor. The effectiveness of this technique is demonstrated by a prototype design of a sampling switch in 0. 35μm. The proposed sampling switch achieves a spurious free dynamic range of 111dB for a 0. 2MHz, 1.2Vp-p input signal, sampled at a rate of 2MS/s,about 18dB over the Bootstrapped switch. Also, the on-resistance variation is reduced by 90%. This method is especially useful for low-voltage, high resolution ADCs, which is a hot topic today.展开更多
A novel charge exchanging compensation (CEC) technique is proposed for a wideband sample-and-hold (S/H) circuit applied in an IF sampling ADC. The CEC technique compensates the sampling bandwidth by eliminating th...A novel charge exchanging compensation (CEC) technique is proposed for a wideband sample-and-hold (S/H) circuit applied in an IF sampling ADC. The CEC technique compensates the sampling bandwidth by eliminating the impact from finite on-resistance of the sampling switch, and avoids increasing clock feedthrough and charge injection. Meanwhile, a low power two stage OTA with a class AB output stage is designed to provide the S/H a 3Vp-p input range under 1.8V power. The S/H achieves a 94dB spurious-free dynamic range for a 200MHz input signal at a 100Ms/s sample rate and consumes only 26mW with a 5.5pF load.展开更多
Power optimization for pipelined analog-to-digital converter(ADC) was studied. Operational principle of pipelined ADC was discussed and noise voltage caused by two important thermal noise sources, sampling switch and ...Power optimization for pipelined analog-to-digital converter(ADC) was studied. Operational principle of pipelined ADC was discussed and noise voltage caused by two important thermal noise sources, sampling switch and amplifier,was quantitatively analyzed. Method used to minimize power and the values under simple model were presented. Power can be saved by making the sampling and feedback capacitors scale down in the pipeline.And the size of capacitors was limited by thermal noise in high resolution ADC.The equivalent circuits of the two important thermal noise sources were established.Thermal noise was optimally distributed among the pipeline stages,and the relationship between scaling factor and closed loop gain was obtained for minimum power dissipation.Typical closed loop gain was 2 or 4 in pipeline ADC, and the corresponding scaling factor was (1.217) and 1.317.These results can serve as useful guidelines for designers to minimize the ADC′s power consumption.展开更多
A 10-bit 250-MSPS two-channel time-interleaved charge-domain(CD) pipelined analog-to-digital converter (ADC) is presented.MOS bucket-brigade device(BBD) based CD pipelined architecture is used to achieve low pow...A 10-bit 250-MSPS two-channel time-interleaved charge-domain(CD) pipelined analog-to-digital converter (ADC) is presented.MOS bucket-brigade device(BBD) based CD pipelined architecture is used to achieve low power consumption.An all digital low power DLL is used to alleviate the timing mismatches and to reduce the aperture jitter.A new bootstrapped MOS switch is designed in the sample and hold circuit to enhance the IF sampling capability.The ADC achieves a spurious free dynamic range(SFDR) of 67.1 dB,signal-to-noise ratio (SNDR) of 55.1 dB for a 10.1 MHz input,and SFDR of 61.6 dB,SNDR of 52.6 dB for a 355 MHz input at full sampling rate.Differential nonlinearity(DNL) is +0.5/-0.4 LSB and integral nonlineariry(INL) is +0.8/-0.75 LSB.Fabricated in a 0.18-μm 1P6M CMOS process,the prototype 10-bit pipelined ADC occupies 1.8×1.3 mm2 of active die area,and consumes only 68 mW at 1.8 V supply.展开更多
文摘A novel, highly linear sampling switch suitable for low-voltage operation is proposed. This switch not only eliminates the nonlinearity introduced by gate-source voltage variation, but also reduces the nonlinearity resuiting from threshold voltage variation, which has not been accomplished in earlier low-voltage sampling switches. This is achieved by adopting a replica transistor with the same threshold voltage as the sampling transistor. The effectiveness of this technique is demonstrated by a prototype design of a sampling switch in 0. 35μm. The proposed sampling switch achieves a spurious free dynamic range of 111dB for a 0. 2MHz, 1.2Vp-p input signal, sampled at a rate of 2MS/s,about 18dB over the Bootstrapped switch. Also, the on-resistance variation is reduced by 90%. This method is especially useful for low-voltage, high resolution ADCs, which is a hot topic today.
文摘A novel charge exchanging compensation (CEC) technique is proposed for a wideband sample-and-hold (S/H) circuit applied in an IF sampling ADC. The CEC technique compensates the sampling bandwidth by eliminating the impact from finite on-resistance of the sampling switch, and avoids increasing clock feedthrough and charge injection. Meanwhile, a low power two stage OTA with a class AB output stage is designed to provide the S/H a 3Vp-p input range under 1.8V power. The S/H achieves a 94dB spurious-free dynamic range for a 200MHz input signal at a 100Ms/s sample rate and consumes only 26mW with a 5.5pF load.
基金Supported by the Tackling Project of Tianjin Science and Technology Committee (No.033183911).
文摘Power optimization for pipelined analog-to-digital converter(ADC) was studied. Operational principle of pipelined ADC was discussed and noise voltage caused by two important thermal noise sources, sampling switch and amplifier,was quantitatively analyzed. Method used to minimize power and the values under simple model were presented. Power can be saved by making the sampling and feedback capacitors scale down in the pipeline.And the size of capacitors was limited by thermal noise in high resolution ADC.The equivalent circuits of the two important thermal noise sources were established.Thermal noise was optimally distributed among the pipeline stages,and the relationship between scaling factor and closed loop gain was obtained for minimum power dissipation.Typical closed loop gain was 2 or 4 in pipeline ADC, and the corresponding scaling factor was (1.217) and 1.317.These results can serve as useful guidelines for designers to minimize the ADC′s power consumption.
基金supported by the National Science Foundation of China(No.61106027)the 333 Talent Project of Jiangsu Province,China(No. BRA2011115)
文摘A 10-bit 250-MSPS two-channel time-interleaved charge-domain(CD) pipelined analog-to-digital converter (ADC) is presented.MOS bucket-brigade device(BBD) based CD pipelined architecture is used to achieve low power consumption.An all digital low power DLL is used to alleviate the timing mismatches and to reduce the aperture jitter.A new bootstrapped MOS switch is designed in the sample and hold circuit to enhance the IF sampling capability.The ADC achieves a spurious free dynamic range(SFDR) of 67.1 dB,signal-to-noise ratio (SNDR) of 55.1 dB for a 10.1 MHz input,and SFDR of 61.6 dB,SNDR of 52.6 dB for a 355 MHz input at full sampling rate.Differential nonlinearity(DNL) is +0.5/-0.4 LSB and integral nonlineariry(INL) is +0.8/-0.75 LSB.Fabricated in a 0.18-μm 1P6M CMOS process,the prototype 10-bit pipelined ADC occupies 1.8×1.3 mm2 of active die area,and consumes only 68 mW at 1.8 V supply.