Domestic wastewater was treated by combined anaerobic biofilm aerobic membrane bioreactor(MBR) process, and part biomass in MBR was withdrawn to treat with ozone, then the ozonated sludge was returned to anaerobic in...Domestic wastewater was treated by combined anaerobic biofilm aerobic membrane bioreactor(MBR) process, and part biomass in MBR was withdrawn to treat with ozone, then the ozonated sludge was returned to anaerobic inlet. In aerobic MBR, MLSS and DO were controlled at 3000—3500 mg/L and 0 8 mg/L respectively. Comparing the experimental results of two stages, it was noticed that ozonation did not affect the removal efficiency for organics but had a significant influence on the removals of NH 3 N and TN. During the ozonation period of two months, no excess sludge was wasted, and a zero sludge yield was obtained.展开更多
Based on the hypothesis of reducing sludge production under cryptic growth conditions, ozone was used as cell lysis agent to treat excess sludge,and then the ozonated supernatant was returned to the aeration tank. The...Based on the hypothesis of reducing sludge production under cryptic growth conditions, ozone was used as cell lysis agent to treat excess sludge,and then the ozonated supernatant was returned to the aeration tank. The results show that COD and NH+4-N removal efficiencies in ozonation process were 87.96% and 84.42%, respectively. Meanwhile, a low excess sludge yield coefficient of 0. 113 ( g SS/g COD removed) was obtained. Compared with that of the control test, the process configuration decreased the excess sludge production by 51.3%.展开更多
文摘Domestic wastewater was treated by combined anaerobic biofilm aerobic membrane bioreactor(MBR) process, and part biomass in MBR was withdrawn to treat with ozone, then the ozonated sludge was returned to anaerobic inlet. In aerobic MBR, MLSS and DO were controlled at 3000—3500 mg/L and 0 8 mg/L respectively. Comparing the experimental results of two stages, it was noticed that ozonation did not affect the removal efficiency for organics but had a significant influence on the removals of NH 3 N and TN. During the ozonation period of two months, no excess sludge was wasted, and a zero sludge yield was obtained.
文摘Based on the hypothesis of reducing sludge production under cryptic growth conditions, ozone was used as cell lysis agent to treat excess sludge,and then the ozonated supernatant was returned to the aeration tank. The results show that COD and NH+4-N removal efficiencies in ozonation process were 87.96% and 84.42%, respectively. Meanwhile, a low excess sludge yield coefficient of 0. 113 ( g SS/g COD removed) was obtained. Compared with that of the control test, the process configuration decreased the excess sludge production by 51.3%.