介绍了蜡油加氢装置的综合能耗组成,对装置能耗组成进行分析,并通过增加热联合利用率、取消燃料油改烧燃料气、高能耗机泵叶轮改造、压缩机增加无级调节系统、装置分馏系统优化操作等节能降耗措施,大幅降低装置综合能耗,从设计能耗17.23...介绍了蜡油加氢装置的综合能耗组成,对装置能耗组成进行分析,并通过增加热联合利用率、取消燃料油改烧燃料气、高能耗机泵叶轮改造、压缩机增加无级调节系统、装置分馏系统优化操作等节能降耗措施,大幅降低装置综合能耗,从设计能耗17.23 kg Eo/t降低至2012年的6.13 kg Eo/t,成效卓著。展开更多
Evolutionary algorithm is applied for distillation separation sequence optimization synthesis problems with combination explosion. The binary tree data structure is used to describe the distillation separation sequenc...Evolutionary algorithm is applied for distillation separation sequence optimization synthesis problems with combination explosion. The binary tree data structure is used to describe the distillation separation sequence, and it is directly applied as the coding method. Genetic operators, which ensure to prohibit illegal filial generations completely, are designed by using the method of graph theory. The crossover operator based on a single parent or two parents is designed successfully. The example shows that the average ratio of search space from evolutionary algorithm with two-parent genetic operation is lower, whereas the rate of successful minimizations from evolutionary algorithm with single parent genetic operation is higher.展开更多
In this work, the extractive distillation with heat integration process is extended to separate the pressure-insensitive benzene-cyclohexane azeotrope by using furfural as the entrainer. The optimal design of extracti...In this work, the extractive distillation with heat integration process is extended to separate the pressure-insensitive benzene-cyclohexane azeotrope by using furfural as the entrainer. The optimal design of extractive distillation process is established to achieve minimum energy requirement using the multi-objective genetic algorithm, and the results show that energy saving for this heat integration process is 15.7%. Finally, the control design is performed to investigate the system's dynamic performance, and three control structures are studied. The pressure-compensated temperature control scheme is proposed based on the first two control structures, and the dynamic responses reveal that the feed disturbances in both flow rate and benzene composition can be mitigated well.展开更多
Internal thermally coupled distillation columns (ITCDIC) are the frontier of distillation energy saving research. In this paper, a novel energy saving model of ideal ITCDIC and a simulation algorithm are presented,upo...Internal thermally coupled distillation columns (ITCDIC) are the frontier of distillation energy saving research. In this paper, a novel energy saving model of ideal ITCDIC and a simulation algorithm are presented,upon which a series of comparative studies on energy savings with conventional distillation columns are carried out. Furthermore, we present an optimization model of ideal ITCDIC, which can be used to achieve the maximum energy saving and find the optimal design parameters directly. The binary system of benzene-toluene is adopted for the illustrative example of simulation and optimization. The results show that the maximum energy saving of ITCDIC is 52.25% (compared with energy consumption of conventional distillation under the minimum reflux ratio operation); the optimal design parameters are obtained, where the rectifying section pressure and the feed thermal condition are Pr=0.3006 MPa and q=0.5107 respectively.展开更多
The simulated process model of the HAc dehydration process under actual overloaded condition was conducted by amending the model of standard condition in our previous work using the process data collected from actual ...The simulated process model of the HAc dehydration process under actual overloaded condition was conducted by amending the model of standard condition in our previous work using the process data collected from actual production. Based on the actual process model, the operation optimization analysis of each plant(HAc dehydration column, decanter and NPA recycle column) was conducted using Residue Curve Maps(RCMs),sensitivity analysis and software optimization module. Based on the optimized parameters, the influence of feed impurity MA and the temperature of decanter on the separating effect and energy consumption of the whole process were analyzed. Then the whole process operation optimizing strategy was proposed with the objective that the total reboiler duty Q Total of C-1 and C-3 reaches the minimum value, keeping C-1 and C-3 at their optimized separation parameters obtained above, connecting all the broken recycle and connection streams, and using the temperature of D-1 as operation variable. The optimization result shows that the total reboiler duty Q Total of the whole process can reach the minimum value of 128.32 × 10~6 k J·h^(-1) when the temperature of decanter is 352.35 K, and it can save 5.94 × 10~6 k J·h^(-1), about 2.56 t·h^(-1) low-pressure saturated vapor.展开更多
Exergy indicates the maximal energy that can do work effectively. Different from optimization of product quality or calculation of generic energy conservation in most previous studies, the application of exergy analys...Exergy indicates the maximal energy that can do work effectively. Different from optimization of product quality or calculation of generic energy conservation in most previous studies, the application of exergy analysis and exergy cost optimization in petrochemical industry is of great economic and environmental significance. Based on the main fractionator in Jiujiang Petrochemical Complex No. 2 FCCU, an enhanced exergy cost optimization under different operating conditions by adjusting set points of temperature and valves opening degree for flow control is studied in this paper in order to reduce exergy cost and improve the quality of energy. A steadystate optimization algorithm to enhance exergy availability and an objective function comprehensively considering exergy loss are proposed. On the basis of ensuring the quality of petroleum products, the economic benefits can be improved by optimizing the controllable variables due to the fact that exergy cost is decreased.展开更多
A new method for the fast detection and evaluation of optimization potentials for separation processes is presented within this work. The method disclaims the application of difficult rigorous mathematical optimizatio...A new method for the fast detection and evaluation of optimization potentials for separation processes is presented within this work. The method disclaims the application of difficult rigorous mathematical optimization techniques by a number of different smart workarounds. The basis for the optimization is the application of different heuristics, shortcut methods and simulation studies. The method was applied to a real process in which the overall yield was improved of about 58%. Due to the new configuration an alternative control scheme containing unusual control loops was implemented.展开更多
文摘Evolutionary algorithm is applied for distillation separation sequence optimization synthesis problems with combination explosion. The binary tree data structure is used to describe the distillation separation sequence, and it is directly applied as the coding method. Genetic operators, which ensure to prohibit illegal filial generations completely, are designed by using the method of graph theory. The crossover operator based on a single parent or two parents is designed successfully. The example shows that the average ratio of search space from evolutionary algorithm with two-parent genetic operation is lower, whereas the rate of successful minimizations from evolutionary algorithm with single parent genetic operation is higher.
基金supported by the National Natural Science Foundation of China(grant number 21476261)the Key Research and Development Plan Project of Shandong Province(grant number 2015GGX107004)
文摘In this work, the extractive distillation with heat integration process is extended to separate the pressure-insensitive benzene-cyclohexane azeotrope by using furfural as the entrainer. The optimal design of extractive distillation process is established to achieve minimum energy requirement using the multi-objective genetic algorithm, and the results show that energy saving for this heat integration process is 15.7%. Finally, the control design is performed to investigate the system's dynamic performance, and three control structures are studied. The pressure-compensated temperature control scheme is proposed based on the first two control structures, and the dynamic responses reveal that the feed disturbances in both flow rate and benzene composition can be mitigated well.
基金Supported by the National Environmental Protection Bureau of P.R.China(Huan-Ke-Ke,1997,No.006,Project 14),China-Japan cooperative project:"Research on energy savings and alleviating environmental burden in petroleum enterprises"of Institute of Industrial
文摘Internal thermally coupled distillation columns (ITCDIC) are the frontier of distillation energy saving research. In this paper, a novel energy saving model of ideal ITCDIC and a simulation algorithm are presented,upon which a series of comparative studies on energy savings with conventional distillation columns are carried out. Furthermore, we present an optimization model of ideal ITCDIC, which can be used to achieve the maximum energy saving and find the optimal design parameters directly. The binary system of benzene-toluene is adopted for the illustrative example of simulation and optimization. The results show that the maximum energy saving of ITCDIC is 52.25% (compared with energy consumption of conventional distillation under the minimum reflux ratio operation); the optimal design parameters are obtained, where the rectifying section pressure and the feed thermal condition are Pr=0.3006 MPa and q=0.5107 respectively.
基金Supported by Shanghai University Youth Teacher Training Program(ZZsl15002)Shanghai Sailing Program(17YF1413100 and 17YF1428300)
文摘The simulated process model of the HAc dehydration process under actual overloaded condition was conducted by amending the model of standard condition in our previous work using the process data collected from actual production. Based on the actual process model, the operation optimization analysis of each plant(HAc dehydration column, decanter and NPA recycle column) was conducted using Residue Curve Maps(RCMs),sensitivity analysis and software optimization module. Based on the optimized parameters, the influence of feed impurity MA and the temperature of decanter on the separating effect and energy consumption of the whole process were analyzed. Then the whole process operation optimizing strategy was proposed with the objective that the total reboiler duty Q Total of C-1 and C-3 reaches the minimum value, keeping C-1 and C-3 at their optimized separation parameters obtained above, connecting all the broken recycle and connection streams, and using the temperature of D-1 as operation variable. The optimization result shows that the total reboiler duty Q Total of the whole process can reach the minimum value of 128.32 × 10~6 k J·h^(-1) when the temperature of decanter is 352.35 K, and it can save 5.94 × 10~6 k J·h^(-1), about 2.56 t·h^(-1) low-pressure saturated vapor.
基金Supported by the National Natural Science Foundation of China(61590924,61673273,61521063)
文摘Exergy indicates the maximal energy that can do work effectively. Different from optimization of product quality or calculation of generic energy conservation in most previous studies, the application of exergy analysis and exergy cost optimization in petrochemical industry is of great economic and environmental significance. Based on the main fractionator in Jiujiang Petrochemical Complex No. 2 FCCU, an enhanced exergy cost optimization under different operating conditions by adjusting set points of temperature and valves opening degree for flow control is studied in this paper in order to reduce exergy cost and improve the quality of energy. A steadystate optimization algorithm to enhance exergy availability and an objective function comprehensively considering exergy loss are proposed. On the basis of ensuring the quality of petroleum products, the economic benefits can be improved by optimizing the controllable variables due to the fact that exergy cost is decreased.
文摘A new method for the fast detection and evaluation of optimization potentials for separation processes is presented within this work. The method disclaims the application of difficult rigorous mathematical optimization techniques by a number of different smart workarounds. The basis for the optimization is the application of different heuristics, shortcut methods and simulation studies. The method was applied to a real process in which the overall yield was improved of about 58%. Due to the new configuration an alternative control scheme containing unusual control loops was implemented.