The first floating platform concept design work for South China Sea is undergoing in DMAR's office now. This tension leg platform has potential to become the first advanced floating production platform project. Pr...The first floating platform concept design work for South China Sea is undergoing in DMAR's office now. This tension leg platform has potential to become the first advanced floating production platform project. Project execution is always a challenge for floating system. This paper focuses on the critical elements of project execution for tension leg platform,and studies potential implications to future oil and gas exploration in South China Sea. There are many factors affecting successful execution of floating system project,including technical issues, engineering management,interface management,etc. There are also failure examples of project execution in the industry. The author has participated 28 large detailed projects and has gained extensive experience on floating projects,with ample hands-on project experiences. A detailed tension leg platform project study example and discussions in depth are presented for future project execution in China deepwater development.展开更多
Mooring systems play an important role for semi-submersible rigs that drill in deepwater.A detailed analysis was carried out on the mooring of a semi-submersible rig that conducted a trial well drilling at a deepwater...Mooring systems play an important role for semi-submersible rigs that drill in deepwater.A detailed analysis was carried out on the mooring of a semi-submersible rig that conducted a trial well drilling at a deepwater location in the South China Sea in 2009.The rig was 30 years old and had a shallow platform with a designed maximum operating water depth of 457 m.Following the mooring analysis,a mooring design was given that requires upgrading of the rig’s original mooring system.The upgrade included several innovations,such as installing eight larger anchors,i.e.replacing the original anchors and inserting an additional 600 m of steel wires with the existing chains.All this was done to enhance the mooring capability of the rig in order for the rig to be held in position to conduct drilling at a water depth of 476 m.The overall duration of the drilling was 50 days and the upgraded mooring system proved to be efficient in achieving the goal of keeping the rig stationary while it was drilling the trial well in the South China Sea.This successful campaign demonstrates that an older semi-submersible rig can take on drilling in deep water after careful design and proper upgrading and modification to the original mooring system.展开更多
文摘The first floating platform concept design work for South China Sea is undergoing in DMAR's office now. This tension leg platform has potential to become the first advanced floating production platform project. Project execution is always a challenge for floating system. This paper focuses on the critical elements of project execution for tension leg platform,and studies potential implications to future oil and gas exploration in South China Sea. There are many factors affecting successful execution of floating system project,including technical issues, engineering management,interface management,etc. There are also failure examples of project execution in the industry. The author has participated 28 large detailed projects and has gained extensive experience on floating projects,with ample hands-on project experiences. A detailed tension leg platform project study example and discussions in depth are presented for future project execution in China deepwater development.
文摘Mooring systems play an important role for semi-submersible rigs that drill in deepwater.A detailed analysis was carried out on the mooring of a semi-submersible rig that conducted a trial well drilling at a deepwater location in the South China Sea in 2009.The rig was 30 years old and had a shallow platform with a designed maximum operating water depth of 457 m.Following the mooring analysis,a mooring design was given that requires upgrading of the rig’s original mooring system.The upgrade included several innovations,such as installing eight larger anchors,i.e.replacing the original anchors and inserting an additional 600 m of steel wires with the existing chains.All this was done to enhance the mooring capability of the rig in order for the rig to be held in position to conduct drilling at a water depth of 476 m.The overall duration of the drilling was 50 days and the upgraded mooring system proved to be efficient in achieving the goal of keeping the rig stationary while it was drilling the trial well in the South China Sea.This successful campaign demonstrates that an older semi-submersible rig can take on drilling in deep water after careful design and proper upgrading and modification to the original mooring system.