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调节阀流量畸变特性补偿的坐标变换法
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作者 李崇祥 连国钧 张根林 《热力发电》 CAS 北大核心 1998年第6期29-32,共4页
调节阀在使用中 ,其流量特性总会发生畸变 ,严重影响调节品质 ,必须进行特性补偿。本文提出了一种基于坐标变换的调节阀畸变特性补偿算法。该算法简单 ,含义清楚 ,易于智能化 。
关键词 调节阀 流量畸变 补偿 坐标变换法
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Numerical Study on the Influence Mechanism of Inlet Distortion on the Stall Margin in a Transonic Axial Rotor 被引量:3
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作者 Scott C.Morris 《Journal of Thermal Science》 SCIE EI CAS CSCD 2012年第3期209-214,共6页
A numerical study is conducted to investigate the influence of inlet flow condition on tip leakage flow (TLF) and stall margin in a transonic axial rotor.A commercial software package FLUENT,is used in the simulation.... A numerical study is conducted to investigate the influence of inlet flow condition on tip leakage flow (TLF) and stall margin in a transonic axial rotor.A commercial software package FLUENT,is used in the simulation.The rotor investigated in this paper is ND_TAC rotor,which is the rotor of one-stage transonic compressor in the University of Notre Dame.Three varied inlet flow conditions are simulated.The inlet boundary condition with hub distortion provides higher axial velocity for the incoming flow near tip region than that for the clean inflow,while the incoming main flow possesses lower axial velocity near the tip region at tip distortion inlet boundary condition.Among the total pressure ratio curves for the three inlet flow conditions,it is found that the hub dis-torted inlet boundary condition improves the stall margin,while the tip distorted inlet boundary condition dete-riorates compressor stability.The axial location of interface between tip leakage flow (TLF) and incoming main flow (MF) in the tip gap and the axial momentum ratio of TLF to MF are further examined.It is demonstrated that the axial momentum balance is the mechanism for interface movement.The hub distorted inflow could de-crease the axial momentum ratio,suppress the movement of the interface between TLF and MF towards blade leading edge plane and thus enhance compressor stability. 展开更多
关键词 Inlet distortion tip leakage flow stall margin axial momentum balance
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Measurement errors and correction of the UAT-2 ultrasonic anemometer 被引量:1
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作者 CHENG Xue Ling PENG Zhen +4 位作者 HU Fei ZENG Qing Cun LUO Wei Dong ZHAO Yi Jun HONG Zhong Xiang 《Science China(Technological Sciences)》 SCIE EI CAS CSCD 2015年第4期677-686,共10页
Two kinds of measurement errors have been observed in the recently developed UAT-2 ultrasonic anemometer.One is the flow distortion produced by a"blocking effect",and the other is the angle of attack caused ... Two kinds of measurement errors have been observed in the recently developed UAT-2 ultrasonic anemometer.One is the flow distortion produced by a"blocking effect",and the other is the angle of attack caused by the vertical misalignment of the instrument.Here,we study these errors and discuss the possible correction methods.Via a wind tunnel experiment and numerical simulation,a 3D calibration matrix was developed to correct the"blocking effect".In the field test,the angle of attack was detected by an inclinometer settled on the reference plane of the anemometer,and the instrumental misalignment or tilt was corrected by a coordinate transformation.The combined use of an inclinometer and the proposed correction method may help find a new approach for vertical velocity correction. 展开更多
关键词 ultrasonic anemometer transducer array blocking effect attack angle INCLINOMETER
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