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钢包脱氧渣做熔剂冶炼硅锰合金的探索
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作者 王振光 金建凡 赵国文 《山东冶金》 CAS 2009年第4期15-16,18,共3页
硅锰合金作为炼钢的常用脱氧剂,在对钢包内的钢水进行脱氧时,生成的脱氧产物SiO2、MnO必然进入高碱度的炉渣中。石横特钢用这种钢渣代替白云石作熔剂生产硅锰合金,年可降低生产成本36.4万元,回收锰184.366t,达到了资源重复利用、降低成... 硅锰合金作为炼钢的常用脱氧剂,在对钢包内的钢水进行脱氧时,生成的脱氧产物SiO2、MnO必然进入高碱度的炉渣中。石横特钢用这种钢渣代替白云石作熔剂生产硅锰合金,年可降低生产成本36.4万元,回收锰184.366t,达到了资源重复利用、降低成本的目的。同时指出,尽可能地提高脱氧钢渣中的锰含量是进一步的研究方向,"富锰钢渣"有良好的应用前景。 展开更多
关键词 钢包脱氧 熔剂 硅锰合金 白云石
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炼钢大数据影响因素浅析 被引量:4
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作者 赵显久 张捷宇 黄锦锋 《冶金经济与管理》 2019年第2期26-28,共3页
在炼钢生产过程中,常存在当发生了成本、质量上的异常,但却找不到原因的现象,可能的原因是生产工艺和设备参数的相关数据未采集到,或者是对数据的分析不到位。针对转炉停吹游离氧在精炼处理前的游离氧值降低量,以及连铸铝损进行具体分析... 在炼钢生产过程中,常存在当发生了成本、质量上的异常,但却找不到原因的现象,可能的原因是生产工艺和设备参数的相关数据未采集到,或者是对数据的分析不到位。针对转炉停吹游离氧在精炼处理前的游离氧值降低量,以及连铸铝损进行具体分析,以此启发业内相关人员在大数据时代更好地利用数据挖掘并探索冶金相关机理。 展开更多
关键词 转炉 渣脱氧 连铸 中间包 氩封
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LF精炼炉脱硫效率生产实践
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作者 张立明 佟俊梁 +1 位作者 范业广 陈宏杰 《黑龙江冶金》 2012年第1期40-41,43,共3页
对影响钢水脱硫的热力学因素和动力学因素进行了分析讨论,并结合北兴公司的实际和品种特点,从转炉冶炼控制,LF快速化渣、造渣,精炼温度,底吹氩流量,钢-渣脱氧,合理选择精炼渣系以及优化炉渣成分等方面提出了LF精炼脱硫的技术措施。
关键词 LF 钢水脱硫 碱度 钢-渣脱氧
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Combustion and NO_x Emission Behavior of Chinese Coals 被引量:3
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作者 陈宏刚 谢克昌 《Chinese Journal of Chemical Engineering》 SCIE EI CAS CSCD 2002年第3期333-338,共6页
Seven Chinese coals ranking from anthracite to sub-bituminous fromthe Shanxi province were selected for study to forecast thecombustion and NO_x emission behavior. Three UK, one Indonesia andone South Africa coal was ... Seven Chinese coals ranking from anthracite to sub-bituminous fromthe Shanxi province were selected for study to forecast thecombustion and NO_x emission behavior. Three UK, one Indonesia andone South Africa coal was included in the study for reference. A flatflame-turbulent jet apparatus was employed to assess flame stability,ignition performance and NO_x emission behavior for the initial stageof devolatilization and combustion. This apparatus can simulateparticle heating rates, maximum temperatures and the influence of theturbulent Fluid interactions on the fate of volatiles. 展开更多
关键词 DEVOLATILIZATION char reactivity SLAGGING NO_x
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Iron and copper recovery from copper slags through smelting with waste cathode carbon from aluminium electrolysis 被引量:4
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作者 MAO Kai-xuan LI Lei XU Miao 《Journal of Central South University》 SCIE EI CAS CSCD 2021年第7期2010-2021,共12页
To recover metal from copper slags,a new process involving two steps of oxidative desulfurization followed by smelting reduction was proposed in which one hazardous waste(waste cathode carbon)was used to treat another... To recover metal from copper slags,a new process involving two steps of oxidative desulfurization followed by smelting reduction was proposed in which one hazardous waste(waste cathode carbon)was used to treat another(copper slags).The waste cathode carbon is used not only as a reducing agent but also as a fluxing agent to decrease slag melting point.Upon holding for 60 min in air atmosphere first and then smelting with 14.4 wt%waste cathode carbon and 25 wt%CaO for 180 min in high purity Ar atmosphere at 1450℃,the recovery rates of Cu and Fe reach 95.89%and 94.64%,respectively,and meanwhile greater than 90%of the fluoride from waste cathode carbon is transferred into the final slag as CaF_(2) and Ca_(2)Si_(2)F_(2)O_(7),which makes the content of soluble F in the slag meet the national emission standard.Besides,the sulphur content in the obtained Fe-Cu alloy is low to 0.03 wt%. 展开更多
关键词 copper slags waste cathode carbon oxidative desulfurization smelting reduction iron and copper recovery fluoride
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Deoxidation of H13 tool steel with CaF_(2)-MgO-CaO-Al_(2)O_(3)-SiO_(2) slags at 1873 K 被引量:1
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作者 LI Shao-ying LI Bin +3 位作者 DUAN Sheng-chao ZHAO Xing-ming GUO Jing GUO Han-jie 《Journal of Central South University》 SCIE EI CAS CSCD 2021年第2期370-385,共16页
Laboratory-scale experiments were performed to investigate the deoxidation of H13 tool steel with CaF_(2)-MgO-Al_(2)O_(3)-CaO-SiO_(2) slags at 1873 K.The calculation of thermodynamics and kinetics was also verified th... Laboratory-scale experiments were performed to investigate the deoxidation of H13 tool steel with CaF_(2)-MgO-Al_(2)O_(3)-CaO-SiO_(2) slags at 1873 K.The calculation of thermodynamics and kinetics was also verified through the experimental results.The results show that[Si]-[O]reaction is the control reaction,and with the increase of basicity of slag,the limitation of deoxidation was decreased.The limitation of deoxidation is the lowest for the slag with basicity of 2.0.Under the conditions of the basicity of 2.0 and the content of CaF_(2) more than 50%,the limitation of deoxidation is less than 10×10^(−6),and it does not depend on the contents of Al_(2)O_(3) and CaF_(2) in slags.The mass transport of oxygen in the metal phase is the rate-controlling step,and the slag composition has no effect on the equilibrium time of deoxidation.Based on this finding,the optimized slag composition is designed and it contains the following components:51.5%CaF_(2),20.3%MgO,16.2%Al_(2)O_(3),8.2%CaO and 3.8%SiO_(2).In the case of the optimized deoxidizing slag,the total oxygen content in H13 steel can be reduced from 25×10^(−6) to 6×10^(−6). 展开更多
关键词 DEOXIDATION H13 tool steel slag-steel interface reaction slag optimization
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Cyanide removal for ultrafine gold cyanide residues by chemical oxidation methods 被引量:2
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作者 Wen-wen HAN Hong-ying YANG Lin-lin TONG 《Transactions of Nonferrous Metals Society of China》 SCIE EI CAS CSCD 2022年第12期4129-4138,共10页
Because of the highly toxic cyanide in the gold cyanide residues,cyanide must be removed for environmental protection.The process mineralogy of residues was studied firstly,and then cyanide removal was carried out by ... Because of the highly toxic cyanide in the gold cyanide residues,cyanide must be removed for environmental protection.The process mineralogy of residues was studied firstly,and then cyanide removal was carried out by three chemical methods.The results showed that the residue mainly contained Si,S and Fe.Pyrite was the main metallic mineral,and the iron-complex cyanides make cyanide removal difficult.The minerals in residues were in ultrafine particle size with high monomer dissociation degrees.In H_(2)O_(2)oxidation process,the self-decomposition and side reactions resulted in high consumption of H_(2)O_(2).In Na_(2)S_(2)O_(5)-air oxidation process,the time for complete process was long because of the reactions between Na_(2)S_(2)O_(5)and O_(2).Na_(2)SO_(3)oxidation method was found to be a new method for cyanide removal without air inflation device.The cyanide content was reduced to the national standard level in 90 min at pH 9.0 with optimum Na_(2)SO_(3)dose of 2.0 g/L. 展开更多
关键词 gold cyanide residues process mineralogy cyanide removal H2O2 oxidation Na2SO3 oxidation
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100t LF精炼脱硫生产实践 被引量:2
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作者 赵中福 赵继宇 +1 位作者 李小明 王金平 《中国冶金》 CAS 2009年第4期18-22,共5页
对影响钢水脱硫的热力学因素和动力学因素进行了分析讨论,并结合武钢一炼钢的实际和品种特点,从转炉冶炼控制,LF快速化渣、造渣,精炼温度,底吹氩流量,钢-渣脱氧,合理选择精炼渣系以及优化炉渣成分等方面提出了LF精炼脱硫的技术措施。
关键词 100 t LF 钢水脱硫 碱度 钢-渣脱氧
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低碳低硅钢中氧化物夹杂的控制 被引量:6
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作者 周宏 胡兵 +2 位作者 何维祥 程小利 马立华 《炼钢》 CAS 北大核心 2012年第2期29-31,共3页
重庆钢铁股份有限公司新区炼钢厂结合低碳低硅钢的生产实践,为改善钢水可浇性、避免因中间包水口堵塞而停浇的事故发生,对转炉后搅、顶渣脱氧和RH碳脱氧工艺进行了优化。工艺改进后,转炉终点钢水w(O)降低了127×10-6,渣中w(FeO+MnO)... 重庆钢铁股份有限公司新区炼钢厂结合低碳低硅钢的生产实践,为改善钢水可浇性、避免因中间包水口堵塞而停浇的事故发生,对转炉后搅、顶渣脱氧和RH碳脱氧工艺进行了优化。工艺改进后,转炉终点钢水w(O)降低了127×10-6,渣中w(FeO+MnO)<5%,钢水中铝的加入量减少了0.38~0.43 kg/t,有效降低了钢中氧化物夹杂含量,钢中w(T.O)控制在(14~25)×10-6内。生产实践表明:采用"BOF→RH→CC"工艺路线生产低碳低硅钢,提高了钢水洁净度、单中包连浇炉数达18炉。 展开更多
关键词 低碳低硅钢 氧化物夹杂 转炉后搅 渣脱氧 脱氧
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日钢ML08Al冷镦钢炼钢工艺实践
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作者 杨志雄 马启明 +1 位作者 孙喜发 金智启 《钢铁研究》 CAS 2012年第4期50-52,共3页
介绍了ML08Al冷镦钢在炼钢过程中的控制及生产情况,包括转炉冶炼过程中合金的选择,硅质量分数控制,吹氩站渣脱氧以减轻精炼炉的脱氧造白渣的压力,严格控制成分等。这些措施解决了连铸时水口堵塞问题,实现了ML08Al冷镦钢的批量生产。
关键词 ML08Al钢 渣脱氧 硅质量分数
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