In order to realize tobacco curing with energy saving and emission reduc- ing and lower cost, the waste heat recovering equipment was designed and built on blowing-upward type bulk curing barn. The comparative experim...In order to realize tobacco curing with energy saving and emission reduc- ing and lower cost, the waste heat recovering equipment was designed and built on blowing-upward type bulk curing barn. The comparative experiment of tobacco leaf curing was conducted between a bulk curing barn with waste heat of flue gas and conventional bulk curing barn. The results showed that the effect of saving coal in bulk curing barn with waste heat of flue gas was obvious than the contrast. The coal consumption quantity was 1.531 kg per kg of dry tobacco leaf. The saving coal in bulk curing barn with use waste heat of flue gas was 0.181 kg per kg of dry tobacco leaf than the contrast and saving coal rate was 10.57%. The electricity consumption quantity was 0.593 kWh per kg of dry tobacco leaf. The saving elec- tricity quantity in bulk curing barn with use waste heat of flue gas was 0.022 kWh/kg and the saving electricity rate was 3.58% than the contrast. The saving curing cost was 0.158 yuan per kg of dry tobacco leaf and saving cost rate 9.09% in bulk cur- ing barn with use waste heat of flue gas than the contrast. The appearance quality, grade structure and primary chemical composition had no significant difference be- tween bulk curing barn with use waste heat of flue gas and the contrast.展开更多
A novel tobacco-curing system with a solar-assisted heat pump was proposed.The proposed system has various advantages,such as reducing energy consumption and pollutant emissions and enhancing the stability of system o...A novel tobacco-curing system with a solar-assisted heat pump was proposed.The proposed system has various advantages,such as reducing energy consumption and pollutant emissions and enhancing the stability of system operation.The thermal characteristics of the system under different climate conditions were analyzed,and the economic and environmental benefits of different tobacco-curing technologies were compared.Results indicated that the dehydration rate,the mass flux of exhaust air,and the heat load of the novel tobacco-curing system in different months had similar changes with the baking time,and all reached the maximum in the later stage of color fixing.Compared with the power saving rate of a heat pump tobacco-curing system,that of the novel system reached 25.9%-35.1%.The dry leaf curing cost of the novel system was only 0.86-1.06 yuan/kg,which can reduce the cost by more than 60%compared with traditional coal-burning tobacco-curing systems in China.Compared with other parts of the tobacco leaf,the top leaf had the lowest dry leaf curing cost due to its highest mass of dry leaf.The payback period and the annual CO_(2) emission reduction of the novel system were 3.0-3.7 a and 15586 kg,respectively.展开更多
基金Supported by Hebei Industrial Co.,LTD.of China Tobacco(111201315524)Qiannan Co.LTD.Of Guizhou Industrial Co.,LTD.,China Tobacco([2012]17)~~
文摘In order to realize tobacco curing with energy saving and emission reduc- ing and lower cost, the waste heat recovering equipment was designed and built on blowing-upward type bulk curing barn. The comparative experiment of tobacco leaf curing was conducted between a bulk curing barn with waste heat of flue gas and conventional bulk curing barn. The results showed that the effect of saving coal in bulk curing barn with waste heat of flue gas was obvious than the contrast. The coal consumption quantity was 1.531 kg per kg of dry tobacco leaf. The saving coal in bulk curing barn with use waste heat of flue gas was 0.181 kg per kg of dry tobacco leaf than the contrast and saving coal rate was 10.57%. The electricity consumption quantity was 0.593 kWh per kg of dry tobacco leaf. The saving elec- tricity quantity in bulk curing barn with use waste heat of flue gas was 0.022 kWh/kg and the saving electricity rate was 3.58% than the contrast. The saving curing cost was 0.158 yuan per kg of dry tobacco leaf and saving cost rate 9.09% in bulk cur- ing barn with use waste heat of flue gas than the contrast. The appearance quality, grade structure and primary chemical composition had no significant difference be- tween bulk curing barn with use waste heat of flue gas and the contrast.
基金The National Natural Science Foundation of China(No.51922027).
文摘A novel tobacco-curing system with a solar-assisted heat pump was proposed.The proposed system has various advantages,such as reducing energy consumption and pollutant emissions and enhancing the stability of system operation.The thermal characteristics of the system under different climate conditions were analyzed,and the economic and environmental benefits of different tobacco-curing technologies were compared.Results indicated that the dehydration rate,the mass flux of exhaust air,and the heat load of the novel tobacco-curing system in different months had similar changes with the baking time,and all reached the maximum in the later stage of color fixing.Compared with the power saving rate of a heat pump tobacco-curing system,that of the novel system reached 25.9%-35.1%.The dry leaf curing cost of the novel system was only 0.86-1.06 yuan/kg,which can reduce the cost by more than 60%compared with traditional coal-burning tobacco-curing systems in China.Compared with other parts of the tobacco leaf,the top leaf had the lowest dry leaf curing cost due to its highest mass of dry leaf.The payback period and the annual CO_(2) emission reduction of the novel system were 3.0-3.7 a and 15586 kg,respectively.