为了早期发现电力变压器的振动故障问题,需要选择有效位置对变压器的振动状态进行检测。针对电力变压器铁芯—绕组振动特性,通过有限元分析,仿真得到铁芯—绕组测点位置。以型号为S13—12500/35型油浸式无励磁调压35 k V电力变压器为试...为了早期发现电力变压器的振动故障问题,需要选择有效位置对变压器的振动状态进行检测。针对电力变压器铁芯—绕组振动特性,通过有限元分析,仿真得到铁芯—绕组测点位置。以型号为S13—12500/35型油浸式无励磁调压35 k V电力变压器为试验对象,将光纤Bragg光栅(FBG)振动传感器安装于铁芯—绕组的测点位置,对不同负载下变压器振动信号进行检测与频谱分析,结果表明:变压器振动信号频率集中在100 Hz及其倍频处;在80%,90%,100%负载下,幅频信号100 Hz处的振动幅值随着变压器负载的增大而增大。展开更多
Magnetic-valve controllable reactor(MCR)has characteristics of DC bias and different types of magnetic flux density in the magnetic circuit and winding current distortion.These characteristics not only lead to loss ca...Magnetic-valve controllable reactor(MCR)has characteristics of DC bias and different types of magnetic flux density in the magnetic circuit and winding current distortion.These characteristics not only lead to loss calculation method of MCR different from that of power transformer,but also make it more difficult to calculate the core loss and wingding loss of MCR accurately.Our study combines core partition method with dynamic inverse J-A model to calculate the core loss of MCR.The winding loss coefficient of MCR is proposed,which takes into account the influence of harmonics and magnetic flux leakage on the winding loss of MCR.The result shows that the proposed core loss calculation method and winding loss coefficient are effective and correct for the loss calculation of MCR.展开更多
文摘为了早期发现电力变压器的振动故障问题,需要选择有效位置对变压器的振动状态进行检测。针对电力变压器铁芯—绕组振动特性,通过有限元分析,仿真得到铁芯—绕组测点位置。以型号为S13—12500/35型油浸式无励磁调压35 k V电力变压器为试验对象,将光纤Bragg光栅(FBG)振动传感器安装于铁芯—绕组的测点位置,对不同负载下变压器振动信号进行检测与频谱分析,结果表明:变压器振动信号频率集中在100 Hz及其倍频处;在80%,90%,100%负载下,幅频信号100 Hz处的振动幅值随着变压器负载的增大而增大。
基金National Natural Science Foundation of China(No.51367010)Science and Technology Program of Gansu Province(No.17JR5RA083)Program for Excellent Team of Scientific Research in Lanzhou Jiaotong University(No.201701)。
文摘Magnetic-valve controllable reactor(MCR)has characteristics of DC bias and different types of magnetic flux density in the magnetic circuit and winding current distortion.These characteristics not only lead to loss calculation method of MCR different from that of power transformer,but also make it more difficult to calculate the core loss and wingding loss of MCR accurately.Our study combines core partition method with dynamic inverse J-A model to calculate the core loss of MCR.The winding loss coefficient of MCR is proposed,which takes into account the influence of harmonics and magnetic flux leakage on the winding loss of MCR.The result shows that the proposed core loss calculation method and winding loss coefficient are effective and correct for the loss calculation of MCR.