To improve the quality of high carbon wire rods,combined electromagnetic stirring was introduced in the continuous casting of round billets with a diameter of 250mm at Tianjin Rockcheck Steel Group Co.In this paper,th...To improve the quality of high carbon wire rods,combined electromagnetic stirring was introduced in the continuous casting of round billets with a diameter of 250mm at Tianjin Rockcheck Steel Group Co.In this paper,the positioning of final electromagnetic stirring(F-EMS)was determined by nail-shooting method.Furthermore,the effect of mold electromagnetic stirring(M-EMS)on the macrostructure and internal defects in the round billets was investigated to find out the optimal operating parameters for continuous casting of SWRH 82B round billets.The results show the desirable positioning of F-EMS locates 9.7m below the mold level where the molten steel can be effectively driven by electromagnetic force and disperse central composition segregation.The shrinkage cavity is totally eliminated with the rotational M-EMS.The ratio and index of central composition segregation and center porosity can be reduced significantly. Furthermore,the equiaxed crystal ratio is considerably increased to 64%under 480A/3Hz M-EMS and 500A/10Hz F-EMS. Fine microstructure and mechanical property of wire rod are presented after optimization of combined electromagnetic stirring.Accordingly,the probability of occurrence of cup-cone fracture of wire rod is reduced dramatically.展开更多
In order to reveal the mechanism and condition of void closure in large diameter steel rod during horizontal- vertical (H-V) groove rolling process, a three-dimensional thermomechanicaily coupled finite element mode...In order to reveal the mechanism and condition of void closure in large diameter steel rod during horizontal- vertical (H-V) groove rolling process, a three-dimensional thermomechanicaily coupled finite element model was es- tablished for 9-stand H-V groove rolling process aiming at a 4150 mm steel rod production line. A spherical hole with diameter from 2 to 10 mm was preset into the center of continuous casting billet with a rectangle cross section of 300 mmX 360 mm in this model to simulate the void defect, and then finite element analyses were carried out to observe and quantify the void shape evolution in each pass on the three orthogonal coordinate plane sections. The re- suits showed that the void was formed roughly in the reduction and extension directions, and crushed gradually from spherical shape to an approximate ellipsoid, micro-crack and finally to be closed. A quantitative analysis was carried out by using elliptic radii and closure ratio to describe this evolution process; it indicated that the longest axis of the ellipsoid coincided with the rolling line, and the second and third axes were alternatively ihorizontal and vertical on the exit cross section according to change of the reduction direction in H-V groove. The void closure behavior during H- V rolling was more complicated than that of common horizontal rolling, and the influence of groove type and the ex- tension coefficient on the void closure ratio was presented. Finally, a pilot rolling experiment was performed on a 5- stand H-V experimental mill to verify the numerical simulation results, and the experimental results are in good agree- ment with the numerical simulation results.展开更多
基金Item Sponsored by National Natural Science Foundation of China[No.50834009]the National Natural Science Foundation of China[No.51004038]+1 种基金Key Grant Project of China Ministry of Education(No.311014)the 111 Project of China(No.B07015)
文摘To improve the quality of high carbon wire rods,combined electromagnetic stirring was introduced in the continuous casting of round billets with a diameter of 250mm at Tianjin Rockcheck Steel Group Co.In this paper,the positioning of final electromagnetic stirring(F-EMS)was determined by nail-shooting method.Furthermore,the effect of mold electromagnetic stirring(M-EMS)on the macrostructure and internal defects in the round billets was investigated to find out the optimal operating parameters for continuous casting of SWRH 82B round billets.The results show the desirable positioning of F-EMS locates 9.7m below the mold level where the molten steel can be effectively driven by electromagnetic force and disperse central composition segregation.The shrinkage cavity is totally eliminated with the rotational M-EMS.The ratio and index of central composition segregation and center porosity can be reduced significantly. Furthermore,the equiaxed crystal ratio is considerably increased to 64%under 480A/3Hz M-EMS and 500A/10Hz F-EMS. Fine microstructure and mechanical property of wire rod are presented after optimization of combined electromagnetic stirring.Accordingly,the probability of occurrence of cup-cone fracture of wire rod is reduced dramatically.
基金Sponsored by National Natural Science Foundation of China(51005197,51101136)
文摘In order to reveal the mechanism and condition of void closure in large diameter steel rod during horizontal- vertical (H-V) groove rolling process, a three-dimensional thermomechanicaily coupled finite element model was es- tablished for 9-stand H-V groove rolling process aiming at a 4150 mm steel rod production line. A spherical hole with diameter from 2 to 10 mm was preset into the center of continuous casting billet with a rectangle cross section of 300 mmX 360 mm in this model to simulate the void defect, and then finite element analyses were carried out to observe and quantify the void shape evolution in each pass on the three orthogonal coordinate plane sections. The re- suits showed that the void was formed roughly in the reduction and extension directions, and crushed gradually from spherical shape to an approximate ellipsoid, micro-crack and finally to be closed. A quantitative analysis was carried out by using elliptic radii and closure ratio to describe this evolution process; it indicated that the longest axis of the ellipsoid coincided with the rolling line, and the second and third axes were alternatively ihorizontal and vertical on the exit cross section according to change of the reduction direction in H-V groove. The void closure behavior during H- V rolling was more complicated than that of common horizontal rolling, and the influence of groove type and the ex- tension coefficient on the void closure ratio was presented. Finally, a pilot rolling experiment was performed on a 5- stand H-V experimental mill to verify the numerical simulation results, and the experimental results are in good agree- ment with the numerical simulation results.