期刊文献+
共找到3篇文章
< 1 >
每页显示 20 50 100
Cr-V-Al微合金化SWRH82B钢生产工艺研究 被引量:1
1
作者 白澈力格尔 王忠伟 +1 位作者 牟贝成 博宇 《天津冶金》 CAS 2022年第2期12-15,共4页
SWRH82B是日系牌号的高强度预应力钢绞线用钢,而目前天津荣程联合钢铁集团有限公司实施的JIS G3506日系标准,已无法满足SWRH82BΦ13mm盘条抗拉强度≥1180MPa的市场要求,因此需要在此标准的基础上实施微合金化,以提高盘条抗拉强度。本文... SWRH82B是日系牌号的高强度预应力钢绞线用钢,而目前天津荣程联合钢铁集团有限公司实施的JIS G3506日系标准,已无法满足SWRH82BΦ13mm盘条抗拉强度≥1180MPa的市场要求,因此需要在此标准的基础上实施微合金化,以提高盘条抗拉强度。本文对SWRH82B硬线钢的微合金强化工艺进行了研究,并介绍了SWRH82B钢化学成分和生产工艺控制要点。通过成分Cr-V-Al微合金化,同时对转炉、LF炉、VD炉、连铸、轧钢等操作工艺进行了优化调整,生产的SWRH82BΦ13mm盘条时效后的抗拉强度为1190-1202MPa,断面收缩率为39.0-45%,盘条性能满足了预应力钢绞线的市场要求。 展开更多
关键词 Cr-V-Al微合金化 swrh82b硬线钢 预应力钢绞线 抗拉强度
下载PDF
硬线钢SWRH82B控氮技术研究 被引量:1
2
作者 孙福来 《天津冶金》 CAS 2021年第6期29-32,共4页
氮元素在现有的大多数钢种中是有害元素,虽然它在钢中的含量很少,但是却对钢材的性能有着显著的影响,天津钢铁有限公司在生产SWRH82B硬线钢时也遇到了钢水氮含量高而造成的相应质量问题。本文在炼钢、连铸两方面对钢水中氮含量的影响因... 氮元素在现有的大多数钢种中是有害元素,虽然它在钢中的含量很少,但是却对钢材的性能有着显著的影响,天津钢铁有限公司在生产SWRH82B硬线钢时也遇到了钢水氮含量高而造成的相应质量问题。本文在炼钢、连铸两方面对钢水中氮含量的影响因素进行了分析,并对钢水控氮技术进行了研究。在生产过程中,通过优化转炉冶炼操作和底吹模式,对加入合金中氮元素的检测,对相应工艺环节的隔绝空气的严格控制等措施,使钢水氮含量较之前大幅减少,最终得到性能优良的成品钢。 展开更多
关键词 氮元素控制技术 swrh82b硬线钢 钢包底吹、保护浇铸
下载PDF
Study on rolling process optimization of high carbon steel wire 被引量:1
3
作者 Yu-An Jing Lin Hu +1 位作者 Lihui Wang Jingtao Han 《Journal of University of Science and Technology Beijing》 CSCD 2007年第5期431-436,共6页
The existing problems in the manufacture of SWRH82B high carbon steel wire were discussed by sampling and testing the microstructure and properties of the steel from the workshop. To solve the problems, the experiment... The existing problems in the manufacture of SWRH82B high carbon steel wire were discussed by sampling and testing the microstructure and properties of the steel from the workshop. To solve the problems, the experimental parameters for thermal simulation were optimized, and the thermal simulating experiments were carded out on a Gleeblel500 thermal simulator. The process parameters for the manufacture were optimized after analysis of the data, and the productive experiments were performed after the water box in front of the no-twist blocks was reconstructed, to control the temperature of the loop layer. The results from the productive experiments showed that the cooling rate of 10-15℃/s was reasonable before phase transformation, about 5℃/s during phase transformation, and 600-620℃ was the suitable starting temperature for phase transformation. The ultimate strength of the Ф11.0 mm wire was increased to 1150-1170 MPa with an increase of 20-30 MPa, the percentage reduction of section was to 34%-36% with an increase of 1%-3% by testing the finished products after reconstruction. 展开更多
关键词 high-carbon steel WIRE swrh82b microstructure thermal simulation phase transformation
下载PDF
上一页 1 下一页 到第
使用帮助 返回顶部